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Using the Alternative Delivery CMAR Method to Reline Two 12-ft Diameter Steel Pumping Plant Discharge Pipes and Discharge Manifold Piping at the Central Arizona Project

机译:在亚利桑那州中部项目中,使用替代的交付CMAR方法对两个12英尺直径的钢制抽水厂排水管和排水歧管进行重排

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The Central Arizona Project (CAP) recently completed relining two 12-ft diameter steel pipes and associated manifold systems at the Mark Wilmer Pumping Plant on Lake Havasu in western Arizona, using the construction manager at risk (CMAR) project delivery method. The Mark Wilmer Pumping Plant withdraws about 1.6 million acre-feet (ac-ft) of water each year from the Colorado River and via six pumps lifts the water through two 12-ft diameter steel pipes about 850 ft to the Buckskin Mountain Tunnel. The pumps are arranged in two-sets of three units which allows isolation of three pumps, a single manifold, and a single discharge pipe for maintenance while still operating the other three units and associated valves and piping. The two 144-in diameter steel discharge pipes are each about 2,300 ft long with slopes that vary from about 9° to 45°. The discharge pipes and manifolds were installed with the construction of the pumping plant in the early 1980s, and the pipes and manifolds lined with a hot-applied-cold-tar-enamel (HACTE) in 1982. In 1986, the plant was commissioned and has been moving water for over 30 years. In 2016, the right pipe and manifold was relined, and in 2017 the left pipe and manifold was relined. As part of CAP's ongoing asset management program, the manifolds and discharge pipes have been inspected multiple times, and while it was apparent the HACTE was failing, CAP performed spot repairs of the lining as outages and internal man-power allowed. In 2012, it became evident the lining had reached its end and more than just spot repairs would be required to protect the integrity of the steel pipe. A project was developed to remove the HACTE and replace it with a modern coating system. Due to the physical extremes of the work and short outage window, it was decided to use an outside contractor to perform the work, and rather than use the traditional design-bid-build delivery method, CAP decided to use the CMAR approach. This paper will examine the initial development of the project surrounding the decision to use CMAR, outline the contractor selection process and the pros/cons surrounding that process, discuss the role the selected contractor played in the design (pre-construction services) of the new coatings system, then look at the development (negotiations) of the guaranteed maximum price (GMP), and finally review the delivery of the project. A brief discussion of CMAR versus design-bid-build and how the CAP approaches each will also be included.
机译:亚利桑那州中部项目(CAP)最近使用风险施工经理(CMAR)项目交付方法,完成了亚利桑那州西部哈瓦苏湖Mark Wilmer抽水厂的两根直径12英尺的钢管及相关歧管系统的改型。马克·威尔默抽水厂每年从科罗拉多河抽取约160万英亩-英尺的水,并通过六台泵将水通过两条直径为850英尺的12英尺直径的钢管提升到巴克斯金山隧道。这些泵分为两组,每组三个单元,可以隔离三个泵,单个歧管和单个排放管进行维护,同时仍可以操作其他三个单元以及相关的阀门和管道。两条直径144英寸的钢排水管长约2,300英尺,倾斜度从9°到45°不等。排气管和歧管在1980年代初期随抽水设备的建造而安装,1982年,这些管和歧管衬有热敷冷焦油搪瓷(HACTE)。1986年,该设备投入使用并已有30多年的历史了。 2016年,对右管和歧管进行了改型,2017年,左管和歧管进行了改型。作为CAP正在进行的资产管理计划的一部分,对歧管和排放管进行了多次检查,虽然HACTE显然出现故障,但CAP在停机和内部人力允许的情况下对衬里进行了现场维修。在2012年,很明显衬砌已到尽头,不仅需要现场维修以保护钢管的完整性。开发了一个项目,以删除HACTE,并用现代涂层系统代替它。由于工作的物理极端性和短暂的停工期,因此决定使用外部承包商来执行工作,而CAP决定使用CMAR方法,而不是使用传统的设计—投标—建造交付方法。本文将研究围绕使用CMAR的决定的项目的初始开发,概述承包商的选择过程以及围绕该过程的利弊,讨论选定承包商在新建筑的设计(施工前服务)中所扮演的角色涂料系统,然后查看保证最高价格(GMP)的制定(协商),最后审查项目的交付情况。还将简要讨论CMAR与设计竞标构建以及CAP如何接近每种设计。

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