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Application Research on TorkBuster in Well Yashen 1 of Yumen Oilfield

机译:TorkBuster在玉门油田雅深1井的应用研究。

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To the technical difficulties of slow ROP and low drilling efficiency in Silurian formation of Yumen Oilfield.After investigating on the ROP improvement technologies of domestic and abroad similar formation's characteristics,proposing a drilling test program of torsion and percussion in Silurian formation of Well Yashen 1.The test well section is 3753.00~4108.05m,the accumulative footage of TorkBuster is 355.05m,the actually drilling time is 208.35h,the average ROP is 1.70rn/h.Compared with the offset well,the average ROP is up to 110%.The test results are shown that:TorkBuster eliminates the "stick-slip" phenomenon effectively when the bit cutting the formation,ensures the PDC bit continue to cut the formation effectively,cuts down the drilling cycle and saves the drilling cost.It provides a new guiding ideology to increase ROP in Cretaceous formation ofYumen Oilfield.
机译:针对于玉门油田志留系地层ROP慢,钻井效率低的技术难点,在研究了国内外同类地层特征的ROP改良技术后,提出了雅深1井志留系地层扭转和冲击钻探试验方案。试验井段为3753.00〜4108.05m,TorkBuster累计进尺为355.05m,实际钻井时间为208.35h,平均ROP为1.70rn / h。与偏井相比,平均ROP可达110%试验结果表明:TorkBuster在钻头切割地层时有效地消除了“粘滑”现象,确保PDC钻头继续有效地切割地层,缩短了钻井周期,节省了钻井成本。榆门油田白垩系组提高ROP的新指导思想。

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