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Initial Start-Up and Commissioning of Circulating Dry Scrubber at Cooper Unit 2

机译:库珀2号机组循环干式洗涤塔的初步启动和调试

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J. S. Cooper Unit 2 (Cooper Unit 2), which is owned and operated by East Kentucky Power Cooperative (EKPC), recently completed a multi-pollutant control project that included the installation of a Circulating Dry Scrubber (CDS) that is designed to achieve greater than 95% SO_2 removal with an SO_2 inlet loading of 7.2 lb SO_2/mmBtu. This is the highest design SO_2 loading of any semi-dry scrubber in the U.S. The project also added selective catalytic reduction (SCR) for NO_X control and replaced the existing cold-side electrostatic precipitator with a pulse-jet fabric filter (PJFF) for particulate control. This paper provides operation and emission performance results obtained throughout the CDS commissioning period and elaborates on the operation of the auxiliary equipment including but not limited to the lime hydrators, which produce hydrated lime for the CDS. The performance results presented will provide insight as to whether a semi-dry scrubber can compete with a wet FGD system on a facility that burns a high sulfur coal.
机译:东肯塔基电力合作社(EKPC)拥有并运营的JS库珀2号机组(库珀2号)最近完成了一个多污染物控制项目,其中包括安装循环干式洗涤塔(CDS),旨在实现更大的排放。在7.2磅SO_2 / mmBtu的SO_2入口负载下,去除了95%的SO_2。这是美国任何半干式洗涤塔中最高的SO_2设计负荷。该项目还增加了用于NO_X控制的选择性催化还原(SCR),并用脉冲喷射织物过滤器(PJFF)替代了现有的冷侧静电除尘器控制。本文提供了在CDS调试期间获得的运行和排放性能结果,并详细阐述了辅助设备的运行,这些辅助设备包括但不限于为CDS生成熟石灰的石灰水化器。给出的性能结果将提供关于半干式洗涤塔是否可以与燃烧高硫煤的设施上的湿式烟气脱硫系统竞争的见解。

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