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In-situ Test of Cement-Flyash-Gravel Pile Composite Foundation for Passenger Dedicated Line

机译:客运专线水泥粉煤灰碎石桩复合地基现场试验

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The deformation and stress in-situ monitoring plan of representative section of Wuhan-Guangzhou railway passenger dedicated line in China was introduced. The monitored compressions of piles and soil between piles in different depth were analyzed. Then deformation development trends of piles and soil among piles in CFG pile composite foundation was investigated following the construction processes of railway subgrade, namely, filling, rest of loading, surcharge precompression, unloading surcharge, and so on. Based on the tested vertical stress both of CFG piles and soil among piles, their developing trends were investigated for every construction phase, and the pile-soil stress ratio was researched too. In-situ monitored data shows that: (1) Under the filling height 6.2m, the tested settlement of composite foundation is 15.67mm, which proves CFG pile composite foundation is effective on control settlement of subgrade. (2) The compression of pile is not equal to that of soil among piles during subgrade construction, and their difference reduce gradually as a result of stress adjust in composite foundation, with the pile-soil stress ratio tend to one fixed value.
机译:介绍了武广铁路客运专线代表段的变形和应力现场监测计划。分析了不同深度下桩与桩之间土的受压情况。然后,根据铁路路基的填筑,剩余荷载,超载预压,卸荷附加等施工过程,研究了CFG桩复合地基中桩间土的变形发展趋势。基于CFG桩和桩间土的竖向应力试验,研究了各个施工阶段的CFG桩和桩间土的发展趋势,并研究了桩土应力比。现场监测数据表明:(1)在6.2m的填充高度下,复合地基的试验沉降为15.67mm,证明CFG桩复合地基对路基的控制沉降是有效的。 (2)路基施工中桩的压缩不等于桩间的土,受复合地基应力调整的影响,桩之间的压差逐渐减小,桩土应力比趋于一个固定值。

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