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Testing and diagnostics of power transformer in PT. Indonesia Power Kamojang Geothermal Power Plant unit 1

机译:PT中电源变压器的测试和诊断。印尼电力Kamojang地热发电厂1号机组

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This paper presents testing and diagnostics of 40 MVA, 150/11.8 kV,Ynd5 main transformer and 4 MVA, 11.8/6.3 kV auxiliary transformer on PT. Indonesia Power Kamojang Geothermal Power Plan unit 1, that have been in operations for more than 25 years, since 1982. Although the main and auxiliary power transformer installed have been fulfilled their design life, the concept of simple replacement of power transformer in the system considering it as weak or potential source of trouble is no more valid in the present scenario of financial constraint. Today the paradigm has changed and many efforts are being directed to explore new approach/techniques of testing, monitoring, diagnosis, life assessment and condition evaluation and possibility of extending the life of existing power transformer. In this effort of extending the life of existing power transformer, testing and diagnostics of power transformer conditions become very important step whether it is possible to extend certain time of useful life beyond design life and save investment on new power transformer. This paper mainly asses the life condition of total insulation system of power transformer due to failure of insulation material considered to be major factor in power transformer, Testing and diagnostics done on main and auxiliary power transformer based on Transformer Turn Ratio (TTR) test, Winding Resistance (Rdc) test, Insulation Resistance (IR)Test, Tan delta test, Dissolve Gas Analysis (DGA) test and Dielectric Response Analysis (Dirana) test. This kind of tests gives in depth information regarding power transformer conditions and abnormalities. The test results show that the oil and paper insulation of both power transformers were very wet and need immediate purification. Condition of winding resistance on main power transformer also showed very significant increase value (300%) compare to the previous commissioning data that mean also increasing load losses significantly.
机译:本文介绍了PT上40 MVA,150 / 11.8 kV,Ynd5主变压器和4 MVA,11.8 / 6.3 kV辅助变压器的测试和诊断。印度尼西亚电力Kamojang地热发电计划1号机组,自1982年以来已经运行了25年以上。尽管已安装的主,副电源变压器已达到设计寿命,但考虑到系统中电源变压器的简单更换概念在当前财务紧缩的情况下,它作为弱点或潜在的麻烦根源不再有效。如今,范式已发生变化,并且人们正致力于探索测试,监视,诊断,寿命评估和状态评估的新方法/技术,以及延长现有变压器寿命的可能性。在延长现有电力变压器寿命的努力中,电力变压器条件的测试和诊断变得非常重要,这是否有可能将使用寿命延长到设计寿命以外,并节省对新电力变压器的投资。本文主要评估被认为是电力变压器主要因素的绝缘材料故障导致的电力变压器总绝缘系统的寿命状况,基于变压器匝数比(TTR)测试对主,辅电力变压器进行测试和诊断,绕组电阻(Rdc)测试,绝缘电阻(IR)测试,Tan delta测试,溶解气体分析(DGA)测试和介电响应分析(Dirana)测试。这种测试可深入了解有关电源变压器状况和异常的信息。测试结果表明,两个电力变压器的油和纸绝缘都非常潮湿,需要立即净化。与之前的调试数据相比,主电源变压器的绕组电阻状况也显示出非常显着的增加值(300%),这意味着负载损失也显着增加。

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