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Manual Tubing Rotation Reduces Rod Pumping Failures by 76

机译:手动油管旋转将杆抽故障减少了76%

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A large Illinois oil field implemented the use of a new lowcost manual tubing rotator in 25 marginal oil wells to reducewear failures. Wear failures were indicated by “tubing splits”(Mechanical Wear1) or “corrosion occurring along a straightline due to corrosion inhibitor being wiped off from wear(Corrosion Due to Wear)”. The failure rate was lowered from203 repairs/year to 49 repairs/year (a 76% reduction) for “allfailure mechanisms”. Failures due to “Mechanical Wear orCorrosion Wear” were reduced from 108 repairs/year to 18repairs/year (an 83% reduction). This success yielded over a100% rate of return since the tubing rotator will normally payout after eliminating the first pulling job and requires only 15minutes per year of extra labor. Economics suggest that 100%to 20% investment rate of returns are achievable in wellsfailing once every 24 months or more often (not consideringdowntime losses). Thus, the manual rotator is not just for“problem” wells and significantly reduces wear failures.
机译:伊利诺伊州的一个大型油田实施了新的低压 在25个边际油井中花费手动管道旋转器,以减少 磨损故障。磨损故障由“分叉”表示 (机械磨损1)或“腐蚀沿直线 腐蚀缓蚀剂从磨损中擦掉的原因 (磨损引起的腐蚀)”。故障率从 “所有 失败机制”。由于“机械磨损或 腐蚀磨损”从每年108次维修减少到18次 每年进行维修(减少83%)。这一成功产生了 由于油管旋转器通常会支付100%的回报率 消除了第一个拉拔作业后只需要15个 每年额外的分钟数。经济学建议100% 达到20%的投资回报率 每24个月或更多次失败(不考虑 停机时间损失)。因此,手动旋转器不仅仅用于 “问题”井,大大减少了磨损故障。

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