首页> 外文会议>Conference on thermosense >Effects of Inadequate Pipe Insulation on a Power Plant's Heat Cycle.
【24h】

Effects of Inadequate Pipe Insulation on a Power Plant's Heat Cycle.

机译:管材绝缘不足对发电厂热循环的影响。

获取原文

摘要

In the power generation industry, the efficiency of the plant's heat cycle is crucial in the age of de-regulation. As competition increases, the cost of generating electricity must decrease. To lower costs, nuclear power plants are always looking at ways of recovering lost megawatts. Additionally, plants are striving to maintain high availability, especially during the peak load demands. At the Limerick Generating Station (LGS), the System Manager was tackling both challenges. He determined that Unit #1 Drywell temperatures had been historically higher than Unit #2 Drywell temperatures. The Drywell is a concrete primary containment that houses both the nuclear reactor and recirculation pumps in a Boiling Water Reactor (BWR) plant. A driving force to resolve the higher temperatures was the plant's Technical Specifications which dictate a maximum allowable temperature of 135 deg F in the Drywell. During the summer of 1999 (one of the hottest on record for the East coast), the temperatures in the Unit #1 Drywell approached the maximum allowed by the Technical Specifications. Exceeding this temperature would require Unit #1 to reduce power during a critical demand period or even shut down. During a peak load condition, the loss of generating capabilities could be extremely costly for the utility. In extreme circumstances, as recent as the winter of 2001 in California, customers could be faced with the potential of roaming brown outs due to the reduced capacity on the electrical grid. Based on the System Manager's experience, the heat source was suspected to be from less than adequate insulated pipes in the Drywell. To determine the condition and status of the insulation, infrared was used to inspect the pipes. The ideal condition is to observe the maximum temperatures when the reactor is at 100 percent power, but due to the radiological and atmospheric conditions in the Drywell, the inspection would have to be performed immediately after the reactor was shut down for an outage. The initial inspection of the Drywell piping was limited to 30 minutes due the ambient temperature exceeding 130 deg F. The infrared inspection quickly identified numerous thermal anomalies that included aging and worn insulation, not insulated and inadequately insulated pipes, valves and pipe hangers. Insulation repairs were performed during the outage. Although a visual inspection is adequate in finding pipes not insulated, infrared was needed to identify the specific sections of insulation requiring repair. The post outage results indicated that the Drywell temperature dropped an average of 3 deg F, thus insuring adequate margin for the Drywell temperature Technical Specification requirements.
机译:在发电行业中,植物的热循环的效率在脱节时期至关重要。随着竞争的增加,发电的成本必须减少。为了降低成本,核电厂总是在寻找恢复迷失的兆瓦的方法。此外,植物正在努力保持高可用性,特别是在峰值负荷需求期间。在Limerick生成站(LGS),系统管理器正在解决这两个挑战。他确定单位#1 Drywell温度一直高于单位#2 Drywell温度。 Drywell是一种混凝土主要遏制,可以在沸水反应器(BWR)厂中的核反应堆和再循环泵。解决较高温度的驱动力是植物的技术规范,其在干燥中决定了135°F的最大允许温度。 1999年夏季(东海岸的最热门的一个最热门的一个),单位#1 Drywell的温度接近了技术规范所允许的最大值。超过该温度需要单位#1来减少临界需求期间的功率,甚至关闭。在峰值负载条件期间,为该实用程序的生成功能丢失可能是非常昂贵的。在极端情况下,近期作为2001年冬天在加利福尼亚州的冬季,由于电网上的容量降低,客户可能面临漫游棕色外出的潜力。基于系统经理的经验,怀疑热源从干燥槽中的绝缘管少于足够的绝缘管。为了确定绝缘的状态和状态,红外线用于检查管道。理想条件是观察反应器为100%功率时的最大温度,但由于干燥器中的放射性和大气条件,在反应器被关闭以进行中断后,必须立即进行检查。干燥的管道的初始检查限制为30分钟,由于超过130°F的环境温度超过130°F。红外检查迅速确定了包括老化和磨损的绝缘的许多热异常,而不是绝缘和不充分的绝缘管,阀门和管道悬挂器。在停机期间进行绝缘维修。尽管在寻找管道未绝缘的发现时,目视检查是足够的,但需要红外线来识别需要修复的绝缘部分的特定部分。停电后果结果表明,干燥温度平均下降3°F,从而为干燥温度技术规范要求保险充分利润。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号