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STATIC PIPE BURSTING USING VITRIFIED CLAY JACKING PIPE IN PHOENIX SOILS

机译:使用凤凰土壤中的玻璃化粘土顶管管道破裂的静管

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The City of Phoenix, Ariz., recently elected to perform two large pipe bursting projects; one of these projects utilized vitrified clay jacking pipe as the replacement pipe material. The notice to proceed for the project was given May 12, 2008. The Guaranteed Maximum Price (GMP) for the project is $5,323,524.05. This project represents a first in both (1) the most significant upsize and (2) maximum drive length in the United States using the static pull bursting method with replacement segmental pipe. This project also demonstrates a commendable level of cooperation between equipment manufacturer, product pipe manufacturer, contractor, engineering firm and municipality. One of the first sections replaced included bursting and replacing 1,200 m (3,938 ft) of existing 300 mm (12 inch) VCP with 450 mm (18 inch) VCP. The existing sewer line's capacity had been exceeded due to growth of the contributory service area. The utility corridor encompassing the existing line was congested with other utilities making open cut construction challenging. Trenchless pipe bursting was ultimately chosen because of the adjacent utilities and concern of traffic disruption. Soil conditions in the area proved to be one of the biggest challenges. The original pipe to be burst was bedded in a soft dry silty sand material and installed in a trench width ranging from 1 to 1.5 m (3 to 5 ft) depending on depth. Existing trench depths range from 3 to 6 m (10 to 20 ft) deep. This first segment was successfully completed on June 10, 2008.
机译:The City of Phoenix, Ariz., recently elected to perform two large pipe bursting projects;其中一个项目使用玻璃化粘土顶管作为替代管材。该项目的通知于2008年5月12日给出。该项目的保证最高价格(GMP)为5,323,524.05美元。该项目代表了(1)中的第一个(1)最重要的Upsize和(2)美国最大的驱动长度,使用静态拉动爆破方法与替换节段管道。该项目还展示了设备制造商,产品管道制造商,承包商,工程公司和市政府之间的值得称道的合作水平。替换的第一部分之一包括突破和更换具有450毫米(18英寸)VCP的现有300 mm(12英寸)VCP的1,200米(3,938英尺)。由于缴费服务区的增长,已超出现有的下水道线的容量。包括现有线路的公用事业走廊与其他公用事业公司拥挤,采取开放式削减施工具有挑战性。由于邻近的公用事业和交通中断的关注,最终选择了无齿管爆裂。该地区的土壤条件被证明是最大的挑战之一。待突发的原始管道在柔软的干粉状砂材料中铺有床位,并根据深度安装在1至1.5米(3至5英尺)的沟槽宽度。现有的沟槽深度范围为3至6米(10至20英尺)深。该第一部分于2008年6月10日成功完成。

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