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A Case Study of a Low Overburden Longwall Recovery with Pre-Developed Recovery Entries

机译:具有前发育恢复条目的低覆盖层恢复的案例研究

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The 3 Right pre-developed longwall recovery entry at Signal Peak Energy's Bull Mountain No. 1 mine was designed to prevent the abnormal roof conditions encountered in its first two recovery entries. Unique geological conditions, such as the low overburden of approximately 200 feet and prevalence of roof joints in the sandstone overburden, contribute significantly to abnormal conditions during longwall recovery. The 3 Right recovery entry was 42 ft wide and developed in two stages, 21 ft wide in each stage. The entry roof was reinforced with steel wire mesh/non-metallic recovery mesh, high-capacity primary bolts and cables. After all the support was installed, the entry was completely backfilled with specially designed, cuttable, low-density cement. The roof bolting and backfill design were based on current practices in this mine and successful practices in other mines in the U.S. and Australia. Extensive instrumentation was installed in the recovery entry for continuous monitoring of load transfer as the face approached and cut into the recovery entries. The support design was completely successful with a smooth cut-through on January 29 and 30, 2014, significantly reducing the shield recovery time and meanwhile protecting the safety of miners. Based on actual observance and practices of the 3 Right recovery entry, recommendations on improvement and modifications of roof support for 4 Right recovery room are presented.
机译:在信号峰值能量的公牛山第1号矿的3右开发的Longwall恢复条目旨在防止其前两个恢复条目中遇到的异常屋顶条件。独特的地质条件,如砂岩覆盖的屋顶接头的低覆盖率,屋顶关节的普遍性,在长壁回收期间对异常情况有显着贡献。 3个正确的恢复条目为42英尺宽,并在两个阶段开发,每个阶段21英尺宽。用钢丝网/非金属回收网格,高容量初级螺栓和电缆加固进入屋顶。安装了所有支持后,该条目完全回填,采用特殊设计,可切割,低密度水泥。屋顶螺栓和回填设计基于该矿的现行实践以及美国和澳大利亚其他地雷的成功做法。在恢复条目中安装了广泛的仪器,以便在接近和切入恢复条目时持续监测负载传输。通过2014年1月29日和30日,支持设计完全成功,截至2014年1月29日和30日,显着减少了盾牌恢复时间,同时保护矿工的安全性。基于3个正确恢复条目的实际遵守和实践,提出了关于改进和修改屋顶支撑的建议,对4个正确的恢复室进行了改进和修改。

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