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A study on synthetical relieving plug agent for steam huff-puff wells in watersensible formation

机译:水敏地层蒸汽吞吐油井综合卸堵剂的研究

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A great quantity of crude is heavy crude oil which has been produced by using steam huff-puff method in Liaohe Oil Field. This kind of crude contains a lot of resin-asphaltene and possesses the property of very high viscosity (4537 mPa.s at 50 degree) and specific gravity (0.9566-0.9611). The formation is not only very sensible to water, but also damaged by fluids of drilling mud. Through injecting steam, the production rate was still very low and duration of steam huff-puff was very short because of plugs which were formed by clay swelling and the residual hydrocarbon that produced by volatilization of light fraction of heavy crude around wellbore. This paper offered a synthetical relieving plug agent which is a mixed fluid, containing organic mixed solvent, inorganic acid, surfactant and other additives. The synthetical relieving plug agent (ARP-88O1 and BJ-30) has been successfully used in 37 wells in Shuguang No.48 union, Liaohe Oil Field since April 1989. According to the statistical data, obtained from 33 experiment wells, it has been sown that the ARP - 8801 and BJ-30 synthetical relieving plug agent has excellent relieving plug ability for the heavy crude wells of using steam huff-puff method in watersensible formation. The production rate per well was increased on an average from 0-8.6 tons/day (before treatment) to 6.0-26.7 tons/day (after treatment). The duration of steam huff-puff was increased on an average from 121 days (before treatment) to 218 days (after treatment). The oil/steam ratio increased from 0.41 (before treatment) to 1.17 (after treatment). The cumulative incremental oil production has reached 41704 tons. The application in oil field proved that the method, offered by this pape, is a very nice stimulation treatment for heavy crude wells of injecting steam in the watersensible formation. The mechanism of relieving plug is discussed in this paper also.
机译:辽河油田以蒸汽吞吐法生产的重质原油为大量原油。这种原油含有大量的树脂-沥青质,并具有很高的粘度(50度时为4537 mPa.s)和比重(0.9566-0.9611)的特性。该地层不仅对水非常敏感,而且还受到钻井泥浆流体的破坏。通过注入蒸汽,由于粘土膨胀形成的堵塞和井筒周围重质原油的轻质馏分挥发产生的残余烃,堵塞率仍然很低,蒸汽吞吐的持续时间非常短。本文提供了一种合成的缓解堵塞剂,它是一种混合液,包含有机混合溶剂,无机酸,表面活性剂和其他添加剂。自1989年4月以来,合成疏堵剂(ARP-88O1和BJ-30)已在辽河油田曙光48联合工会的37口井中成功使用。根据统计数据,已从33口实验井获得了数据。认为ARP-8801和BJ-30合成卸压堵漏剂对重质原油井具有很好的卸压堵漏能力,采用蒸汽吞吐法可在水敏地层中使用。每口井的生产率平均从0-8.6吨/天(处理前)增加到6.0-26.7吨/天(处理后)。蒸汽吞吐的持续时间平均从121天(治疗前)增加到218天(治疗后)。油/蒸汽比从0.41(处理前)增加到1.17(处理后)。累计增加石油产量达到41704吨。在油田中的应用证明,该纸浆提供的方法是对在水敏地层中注入蒸汽的重质原油井的很好的增产方法。本文还讨论了塞子的释放机理。

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