首页> 外文会议>International Symposium on Frontiers in Offshore Geotechnics; 20050919-21; Perth(AU) >Evaluation of recovery of wall friction after penetration of skirts with laboratory and field tests
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Evaluation of recovery of wall friction after penetration of skirts with laboratory and field tests

机译:通过实验室和现场测试评估裙部穿入后壁摩擦的恢复

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When skirt suction foundations are installed into cohesive soils, wall friction resistance on skirts reduces due to strength decrease of remolded soil along the skirts and the shear strength gradually recovers through dissipation of excess pore water pressure and thixotropy. Experiments in a laboratory and a field have been conducted to evaluate the recovery for alluvium soft clay in Osaka Bay, Japan. Laboratory tests under 1 g and 25 g fields demonstrate that the pore water pressure dissipation has smaller effect on the recovery of wall friction than thixotropy for the clay. The result of the field tests using a larger scale skirt corresponds with that of the laboratory tests and nearly the same recovery rate of the wall friction is obtained.
机译:当将裙吸基础安装在粘性土壤中时,由于沿裙的重塑土的强度降低,裙上的壁摩擦阻力减小,并且通过消散多余的孔隙水压力和触变性逐渐恢复了抗剪强度。已经在实验室和现场进行了实验,以评估日本大阪湾冲积软土的回收率。在1 g和25 g油田下的实验室测试表明,孔隙水压力耗散对壁摩擦的恢复的影响小于粘土的触变性。使用较大尺寸裙板的现场测试结果与实验室测试相对应,并且获得了几乎相同的壁摩擦恢复率。

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