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Clunie Dam Anchoring Works

机译:克鲁尼大坝锚固工程

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Following the statutory inspection of the Loch Tummel reservoir "matters in the interest of safety" were raised requiring a stability analysis be carried out to check the behaviour of the dam under load from a Probable Maximum Flood (PMF) event and also from a seismic event.rnThe paper describes the analysis; site investigation; subsequent design; and on-site construction works to implement a dam anchoring scheme which meets the requirements of the Qualified Civil Engineer.rnThe analysis and subsequent works carried out to Clunie Dam were required following the 10-yearly statutory inspection under the Reservoirs Act 1975 which was carried out in June 1999 by Dr A K Hughes. Subsequent structural assessments demonstrated that the seismic stability of the dam was adequate, but that under worst case PMF conditions, the abutment sections of the dam were likely to crack becoming grossly unstable and were expected to fail. Further consequence studies and ALARP studies demonstrated justification for implementing strengthening works.
机译:在对法定矿山进行法定检查之后,提出了“出于安全考虑的事项”,要求进行稳定性分析,以检查可能的最大洪水(PMF)事件和地震事件在负载下大坝的行为。 .rn本文描述了分析;现场调查;后续设计;并进行现场施工以实施符合合格土木工程师要求的大坝锚固方案。rn根据1975年《水库法》进行了10年的法定检查后,需要对Clunie大坝进行分析和后续工作。于1999年6月由AK休斯博士提出。随后的结构评估表明,该大坝的地震稳定性是足够的,但在最坏情况下的PMF条件下,该大坝的基台部分可能会开裂,变得非常不稳定,并预计会发生故障。进一步的结果研究和ALARP研究证明了实施加固工程的合理性。

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