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ANALYSIS OF HP2 NOZZLE ASSEMBLY FAILURE OF A GAS TURBINE

机译:燃气轮机HP2喷嘴组件故障的分析

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The HP2 nozzle assembly of one of the process platform failed by plastic deformation of the vanes after an operating life of 20,000 hours. The vanes were made of alloy 31. The failed vanes were subjected to detailed failure analysis by conducting metallography, hardness testing, energy dispersive spectroscopy, x-ray diffraction and electron probe micro analysis. The phenomenon of sulphidation and catastrophic oxidation was not observed in the material. It was found that the material had undergone high temperature oxidation. The material did not show any signs of creep damage and phase growth .Preferential attack of carbides was identified. The alloy exhibited loss of hardness at the aerofoil surface which aided material erosion and degradation of alloy strength properties. Various thermal barrier coatings to prevent high temperature oxidation were studied.
机译:其中一个处理平台的HP2喷嘴组件在20,000小时的使用寿命后,由于叶片的塑性变形而失效。叶片由合金31制成。对失效的叶片进行了金相分析,硬度测试,能量色散光谱,X射线衍射和电子探针显微分析,以进行详细的失效分析。在该材料中未观察到硫化和灾难性氧化的现象。发现该材料已经历高温氧化。该材料没有任何蠕变损伤和相生长的迹象。确定了碳化物的优先腐蚀。合金在翼型表面表现出硬度损失,这有助于材料腐蚀和合金强度性能下降。研究了各种防止高温氧化的隔热涂层。

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