首页> 外文会议>Annual North American Waste to Energy Conference(ANWTEC 12); 20040517-20040519; Savannah,GA; US >IMPROVEMENT IN OPERATING AND MAINTENANCE COST WITH A FABRIC FILTER CONVERSION USING POLYTETRAFLUOROETHYLENE (PTFE) MEMBRANE FILTER MEDIA
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IMPROVEMENT IN OPERATING AND MAINTENANCE COST WITH A FABRIC FILTER CONVERSION USING POLYTETRAFLUOROETHYLENE (PTFE) MEMBRANE FILTER MEDIA

机译:使用聚四氟乙烯(PTFE)膜过滤介质进行织物过滤器转化的操作和维护成本的改进

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Wheelabrator Technologies is owner and operator of the 2250 ton per day North Broward County, Florida, facility. The plant consists of three lines rated at 750 tons/day. Each line is equipped with a spray dryer absorber/fabric filter. The original fabric filter design was a shake-deflate baghouse with ten compartments of 180 bags each. The typical bag life was one year with the shake-deflate baghouse using standard woven fiberglass bags. Frequent bag failures led to high operating and maintenance cost for the system. The initial upgrade was a conversion from a shake-deflate baghouse to a reverse-air baghouse with sonic horns. The resultant bag life was improved to two years, which represented a significant reduction in maintenance cost. The latest upgrade for the baghouse system was the installation of PTFE membrane/fiberglass filter bags. The change in the filter media resulted in a dramatic improvement in performance. The baghouse cleaning frequency dropped from 360 cycles per day to approximately 50 cycles per day. The average differential pressure across the baghouse system also dropped by 6 in. w. g. The membrane filter bags have achieved over two years life to date and have significantly reduced operating and maintenance costs associated with the baghouse. This paper will detail the steps taken in the conversion from the original shake-deflate design using standard filter bags to the reverse-air with sonic horns using membrane bags. An analysis of the cost of the upgrades and subsequent savings for each step will be included.
机译:Wheelabrator Technologies是佛罗里达州北布劳沃德县日产量2250吨的设施的所有者和经营者。该工厂由三条生产线组成,日产量为750吨。每条生产线均配有喷雾干燥吸收器/织物过滤器。最初的织物过滤器设计是一个摇晃放气的布袋除尘器,每袋有十个隔室,每个袋有180个袋。使用标准编织玻璃纤维袋的振动放气袋式除尘器,典型的袋寿命为一年。频繁的袋子故障导致系统的高昂运营和维护成本。最初的升级是从摇头放气的布袋除尘器转换为带有声角的反向空气布袋除尘器。最终的袋子寿命提高到两年,这意味着维护成本大大降低。布袋除尘系统的最新升级是安装PTFE膜/玻璃纤维滤袋。过滤介质的变化导致性能的显着提高。布袋除尘器的清洁频率从每天360个循环下降到每天大约50个循环。布袋除尘器系统上的平均压差也下降了6英寸瓦。 G。迄今为止,膜滤袋的使用寿命已超过两年,并且大大降低了与集尘室相关的操作和维护成本。本文将详细介绍转换过程,从使用标准滤袋的原始振动放气设计到使用膜袋的带有声音喇叭的反向空气转换的步骤。将包括对升级成本和每个步骤的后续节省的分析。

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