首页> 美国政府科技报告 >Tests of Submerged Duct Installation on the Ryan FR-1 Airplane in the Ames 40- by 80-Foot Wind Tunnel
【24h】

Tests of Submerged Duct Installation on the Ryan FR-1 Airplane in the Ames 40- by 80-Foot Wind Tunnel

机译:在ames 40-80英尺风洞中的Ryan FR-1飞机上安装水下导管的测试

获取原文

摘要

An investigation of an NACA submerged intake installation on the Ryan FR-1 was conducted to determine the full-scale aerodynamic characteristics of this installation. In addition, tests were conducted on the submerged inlet with revised entrance lips and deflectors to determine the configuration which would result in the best dynamic pressure recovery measured at the inlet for this installation without a major rework of the entrance. Stalling of the air flow over the inner lip surface created excessive dynamic pressure losses with the original entrance. The revised entrance produced a 12-percent increase in dynamic pressure recovery at the design high-speed inlet-velocity ratio and resulted in an improvement of thte critical-speed characteristics of the entrance lip. A complete redesign of the entrance including a decrease in ramp angle and adjustment of lip camber is necessary to secure optimum results from this submerged duct installation.

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号