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Evaluation of SCC Test Methods for Inconel 600 in Low Temperature Aqueous Solutions

机译:Inconel 600在低温水溶液中sCC测试方法的评价

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In late 1981, widespread leakage was encountered in Alloy 600 steam-generator tubing at the Three Mile Island Unit 1 nuclear power plant. The phenomenon was identified as low-temperature intergranular stress-corrosion cracking (SCC) initiated from the inner surfaces of the tubes exposed to the primary coolant. A testing program was initiated to examine the material and environmental factors relevant to these failures, which were found to be associated with sensitization of the material and contamination of the coolant by air and sodium thiosulfate. The test solutions contained 1.3% boric acid with various additions of sulfur compounds and lithium hydroxide. Constant extension rate testing was used as the primary tool to examine environmental effects such as the inhibition of cracking by lithium hydroxide. Important effects of crack-initiation frequency on the specimen potential (and therefore crack velocity) are demonstrated. (ERA citation 08:033668)

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