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Investigation of Feasibility of Integral Gas Turbine Engine Solid Particle Inlet Separators. Phase II. Feasibility Demonstration.

机译:整体式燃气轮机发动机固体颗粒进口分离器可行性研究。第二阶段。可行性演示。

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Two different sand and dust particle separator test rigs were fabricated and tested to evaluate separation efficiency,aerodynamic performance characteristics,and operation in rain and foliage ingestion conditions. The semi-reverse-flow separator utilized fixed turning vanes on a contoured hub to induce swirl in an annular duct. At design airflow of 8lb/sec and 40% scavenge flow,the semi-reverse-flow separator demonstrated 88.5% separation efficiency with AC coarse test dust at an average pressure drop of 2.8in. H2O. The powered mixed-flow separator attempted to utilize the strong centrifugal field available in a mixed-flow impeller turning at the high speeds characteristic of small gas turbine engines to achieve particle separation. At the design airflow of 8lb/sec,it demonstrated a maximum separation efficiency of 58.7% with 8.4% scavenge flow and an average pressure rise of 6.76psi. Both separator concepts were determined to be feasible and the semi-reverse-flow separator is considered to be superior to current engine air particle separators for the majority of aspects investigated. (Author)

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