首页> 外文期刊>Tunnelling and underground space technology >Optimization study on the reconstruction and expansion of an underground rail transit center in Shanghai soft ground
【24h】

Optimization study on the reconstruction and expansion of an underground rail transit center in Shanghai soft ground

机译:上海软土地下轨道交通中心改扩建的优化研究。

获取原文
获取原文并翻译 | 示例
       

摘要

To meet the demand of rapid growing passenger flow, Shanghai-Century-Avenue-Transit-Center (SCATC) was reconstructed to integrate two new metro stations with the existing ones. The entire reconstruction process of SCATC involved a cluster of complicated construction cases and procedures including dismantling and restructuring of old station structures as well as deep excavations. In order to control the disturbance of the reconstruction to a minimum, a series of numerical simulations coupling with system control conceptions were conducted for optimizing the reconstruction process. All the involved major cases and their included procedures had been identified and thoroughly investigated to ensure that the incremental effect of each step and overall impact on the old or remaining stations were all within the control criterion for metro operation. The primary findings obtained were: (1) An approach of coupling system control conceptions with numerical simulations incorporated updating procedures was conducted to determine the optimal sequence for the reconstruction, and proved to be efficient and pragmatic; (2) A robust anti-upheaval system was applied and proved very effective in reducing the upheaval effects induced by dismantling structures. With the help of the anti-upheaval system, the displacements induced by subsequent actions had also been reduced much more than expected; (3) In the cutting-hole procedure on walls, by setting the hole size of per-cutting within 1 m and the hole-spacing of no less than 4 m with compensating measures for concentrated forces, the potential damages to the station structures had been prevented effectively; (4) By dividing the large pit into small independent pits with compartment walls, excavating each individual pit and forming its inside structures separately before the adjacent pit started, the rail displacement induced by the large pit excavation had been controlled within 10 mm in Shanghai soft ground; (5) The optimal overall sequence for the SCATC reconstruction was determined by investigating and comparing the effects of all construction paths defined by permutation of the major cases. The optimal sequence was executed and proved successful by the field measurements and observations.
机译:为了满足快速增长的客流需求,上海世纪大道转乘中心(SCATC)进行了改造,将两个新的地铁站与现有的地铁站整合在一起。 SCATC的整个重建过程涉及一系列复杂的施工案例和程序,包括旧车站结构的拆除和改建以及深挖。为了将重建的干扰降到最低,进行了一系列与系统控制概念相结合的数值模拟,以优化重建过程。确定并彻底调查了所有涉及的重大案件及其包括的程序,以确保每个步骤的增量影响以及对旧车站或剩余车站的总体影响都在地铁运营的控制标准之内。得到的主要发现是:(1)采用一种结合了更新程序的数值模拟与系统控制概念相结合的方法,确定了重建的最佳顺序,并被证明是有效且务实的; (2)应用了强大的抗剧变系统,并被证明在减少因拆除结构而引起的剧变效果方面非常有效。在反动荡系统的帮助下,后续行动所引起的流离失所也大大减少。 (3)在墙壁上的开孔步骤中,通过将每次开孔的孔径设置在1 m以内,并通过集中力的补偿措施将开孔间隔设置为不少于4 m,对站台结构的潜在破坏是有效地预防(4)通过将大坑分成带有隔室壁的小独立坑,开挖每个单独的坑,并在相邻坑开始之前分别形成其内部结构,上海大软坑大坑开挖引起的钢轨位移已控制在10 mm以内地面; (5)通过调查和比较主要案例排列确定的所有施工路径的影响,确定SCATC重建的最佳总体顺序。执行最佳顺序并通过现场测量和观察证明是成功的。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号