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首页> 外文期刊>Tunnelling and underground space technology >A pilot study for retrospective evaluation of cured-in-place pipe (CIPP) rehabilitation of municipal gravity sewers
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A pilot study for retrospective evaluation of cured-in-place pipe (CIPP) rehabilitation of municipal gravity sewers

机译:对市政重力下水道的现浇管(CIPP)修复进行回顾性评估的初步研究

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摘要

Pipe rehabilitation and trenchless pipe replacement technologies have seen a steadily increasing use over the past 30-40 years. Despite the massive public investment in the rehabilitation of the US water and wastewater infrastructure, there has been little formal and quantitative evaluation of whether rehabilitation technologies are performing as expected and whether rehabilitation is indeed cost-effective compared to replacement. This paper describes the results of a pilot project for the retrospective evaluation of cured-in-place pipe (CIPP) liners. The pilot testing used CIPP samples from both large and small diameter sewers in two cities: Denver, CO and Columbus, OH. Testing on the liners included: thickness, annular gap, ovality, density, specific gravity, porosity, flexural strength, flexural modulus, tensile strength, tensile modulus, surface hardness, glass transition temperature, and Raman spectroscopy. In addition, environmental data was gathered as appropriate to each retrieval process including: external soil conditions and pH, and internal waste stream pH. Summaries of the test results and a discussion of their implications for CIPP performance are provided in this paper. All of the samples retrieved from the four locations involved in the pilot study testing were in excellent condition after being in use for 25 years, 23 years, 21 years and 5 years, respectively. Overall, it is concluded that there is no reason to anticipate that the liners evaluated in this pilot study will not last for their intended lifetime of 50 years and perhaps well beyond.
机译:在过去的30-40年中,管道修复和非开挖管道更换技术的使用稳步增长。尽管在美国水和废水基础设施的修复方面投入了大量公共资金,但很少有正式和定量的评估来评估修复技术是否按预期进行,以及与替代相比修复是否确实具有成本效益。本文介绍了对就地固化管道(CIPP)衬管进行回顾性评估的试点项目的结果。试点测试使用了来自两个城市(科罗拉多州丹佛和俄亥俄州哥伦布)的大直径和小直径下水道的CIPP样品。对衬板的测试包括:厚度,环形间隙,椭圆度,密度,比重,孔隙率,弯曲强度,弯曲模量,拉伸强度,拉伸模量,表面硬度,玻璃化转变温度和拉曼光谱。此外,针对每个检索过程适当收集了环境数据,包括:外部土壤条件和pH值以及内部废物流的pH值。本文提供了测试结果的摘要及其对CIPP性能的影响的讨论。从参与初步研究测试的四个位置取回的所有样品分别在使用25年,23年,21年和5年后处于良好状态。总体而言,得出的结论是,没有理由预期在该初步研究中评估的衬管将不会持续其预期的50年使用寿命,甚至可能更长。

著录项

  • 来源
    《Tunnelling and underground space technology》 |2014年第1期|82-93|共12页
  • 作者单位

    Trenchless Technology Center, Louisiana Tech University, P.O. Box 10348, Ruston, LA 71272, United States;

    Trenchless Technology Center, Louisiana Tech University, P.O. Box 10348, Ruston, LA 71272, United States;

    Trenchless Technology Center, Louisiana Tech University, P.O. Box 10348, Ruston, LA 71272, United States;

    Trenchless Technology Center, Louisiana Tech University, P.O. Box 10348, Ruston, LA 71272, United States;

    Battelle Memorial Institute, Battelle, 505 King Avenue, Columbus, OH 43201, United States;

    Battelle Memorial Institute, Battelle, 505 King Avenue, Columbus, OH 43201, United States;

    US Environmental Protection Agency, Urban Watershed Branch, National Risk Management Research Laboratory, Water Supply and Water Resources Division, 2890 Woodbridge Avenue (MS-104), Edison, NJ 08837, United States;

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  • 原文格式 PDF
  • 正文语种 eng
  • 中图分类
  • 关键词

    CIPP; Rehabilitation; Sewer; Testing; Evaluation; Deterioration; QA/QC; Assessment;

    机译:CIPP;复原;下水道;测试;评估;恶化;质量检查/质量控制;评定;

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