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Evaluation of Sand-Control Completions in the Duri Steamflood Sumatra, Indonesia

机译:在印度尼西亚苏门答腊杜里蒸汽驱的防砂完工评估

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The Duri field in Sumatra, Indonesia, shown in Fig. 1 and operated by Chevron Pacific Indonesia (CPI), is one of the largest onshore steamflood operations in the world. Producing heavy oil (approximately 25° API) from an essentially unconsolidated reservoir with a depth that ranges from 300 to 700 ft using steam injection at 300 to 400℉ poses a unique challenge in designing an effective, yet economic, completion. One of the biggest problems associated with the production of the crude oil in this environment is the production of massive amounts of solids. In addition to the cost of the recompletions, problems associated with disposing of this amount of sand-and the effect the produced solids have on the facilities, such as stabilization of emulsions-are a large cost to operations.rnA program was initiated in 2002 to evaluate the effectiveness of the completions in the Duri field. This effort involved evaluated field data, such as the frequency and type of workovers, the amount and size of produced solids, the nature and number of failed liners, and the frequency of stuck sucker-rod pumps, to understand the efficiency of the sand-control completions better. Local sand-control gravel used in the completions was evaluated for steam dissolution and adherence to American Petroleum Institute (API) gravel-pack-sand standards. An audit of the primary sand-control-screen manufacturer was also conducted to evaluate the quality of the sand-control screens used in the completions. In addition, on-site inspections of the operational aspects of the completions were completed. The results of the program showed that the completion designs and sand-control screens were up to industry standards. However, several operational aspects were identified as opportunities for improvement. The results of the program are presented, and items for improvement of the completion for thermal wells in the Duri field are discussed in this paper.
机译:如图1所示,印度尼西亚雪佛龙太平洋公司(CPI)运营的印度尼西亚苏门答腊Duri油田是世界上最大的陆上蒸汽驱业务之一。在300到400℉的蒸汽注入下,从一个基本未固结的油层中开采深度为300到700 ft的稠油(API大约25°),在设计有效而经济的完井过程中面临着独特的挑战。在这种环境下与原油生产相关的最大问题之一是大量固体的生产。除了重新装填的费用外,与处理这种数量的沙子有关的问题以及所产生的固体物对设施的影响(例如乳液的稳定化)也是运营的一大费用。2002年启动了一项计划,评估Duri油田完井的有效性。这项工作涉及评估现场数据,例如修井的频率和类型,产生的固体的数量和大小,失效衬管的性质和数量以及抽油杆泵的频率,以了解砂子的效率。控制完工效果更好。对完井中使用的当地防砂砾石进行了蒸汽溶解性评估,并评估了其是否符合美国石油学会(API)砾石充填砂标准。还对主要的防砂筛网制造商进行了审核,以评估完井中使用的防砂筛网的质量。此外,还完成了对完井作业方面的现场检查。该计划的结果表明,完井设计和防砂筛达到了行业标准。但是,一些操作方面被确定为改进的机会。介绍了该计划的结果,并讨论了改善Duri油田热井完井的项目。

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