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Effect of in-situ sample quality on undrained cyclic strength and liquefaction assessment

机译:原位样品质量对不排水循环强度和液化评估的影响

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摘要

This study investigates the effects of quality of in-situ sandy samples, which were taken by a conventional tube sampling (TS) method, on liquefaction assessment. The sandy samples were retrieved from a loose fill layer and medium-dense Holocene deposit in young reclaimed land in Urayasu City where significant liquefaction occurred during the 2011 off the Pacific Coast of Tohoku Earthquake. First, a series of small strain measurements and undrained cyclic triaxial tests was conducted on the TS and reconstituted samples. Second, in order to investigate an applicability of the tested samples for the liquefaction assessment, an effective stress analysis was performed by use of soil parameters obtained from the examined samples. Input earthquake motions of the analysis are the 2011 off the Pacific Coast of Tohoku Earthquake and the 1987 Chiba Toho-oki Earthquake, the first and the second largest earthquakes the investigation site has experienced. The result of a sample quality assessment with the small strain shear moduli indicates that the TS sample retrieved from the Holocene deposit remains of high quality. In addition, for the reconstituted sample of the fill layer, since the small strain shear moduli of the sample are found to be nearly equal to those obtained at the field, it can be considered that the in-situ soil structure condition is reproduced in the reconstituted sample. According to an official report, the liquefaction resistance of the TS sample of the loose fill layer is R-L20 = 0.3 8, which is much larger than that of medium-dense Holocene deposit (R-L20 = 0.29) measured in this study. This is because the fill layer is so loose that the TS sample could have been strengthened due to disturbance during the sampling. On the other hand, the test result for the reconstituted sample of fill layer shows an appropriate level of liquefaction resistance (R-L20 = 0.14). The results of the effective stress analysis using the soil parameters obtained from the TS sample of Holocene deposit and the reconstituted sample of fill layer show the most probable behaviors of the ground at the investigation site for both the 2011 off the Pacific Coast of Tohoku Earthquake and the 1987 Chiba Toho-oki Earthquake, which are consistent with the evidence reported after the earthquakes. The results indicate that the sample quality assessment by using a small strain shear moduli is applicable for the rational liquefaction assessment, and it would be possible to employ the reconstituted sample, which the small strain shear moduli are the same with the in-situ value, in substitution for a high quality sample. (C) 2016 The Japanese Geotechnical Society. Production and hosting by Elsevier B.V.
机译:这项研究调查了通过常规试管采样(TS)方法采集的原位砂土样品的质量对液化评估的影响。砂岩样品取材于浦安市年轻填海区的一个松散填充层和中等密度全新世沉积物中,该地区在2011年东北太平洋地震中发生了严重的液化。首先,对TS和重组样品进行了一系列小应变测量和不排水循环三轴测试。其次,为了研究测试样品在液化性评估中的适用性,使用从测试样品中获得的土壤参数进行了有效的应力分析。分析的输入地震运动是2011年东北太平洋海岸地震和1987年千叶东邦冲木地震,这是该调查地点经历的第一场和第二场地震。小应变剪切模量的样品质量评估结果表明,从全新世沉积物中取回的TS样品保持高质量。另外,对于填充层的重构样品,由于发现样品的小应变剪切模量几乎等于在现场获得的那些,因此可以认为在土壤中再现了原位土壤结构条件。重构样品。根据官方报告,松散填充层的TS样品的抗液化性为R-L20 = 0.3 8,比本研究中测量的中密度全新世沉积物(R-L20 = 0.29)大得多。这是因为填充层太松,以致于TS样本可能由于采样期间的干扰而得到加强。另一方面,对填充层的重构样品的测试结果显示出适当水平的抗液化性(R-L20 = 0.14)。使用全新世沉积物TS样品和填充层重构样品获得的土壤参数进行的有效应力分析结果表明,2011年东北太平洋海岸地震和2011年东北太平洋地震在调查地点的地面最可能表现为1987年千叶县东宝木地震,与地震后报道的证据一致。结果表明,采用小应变剪切模量的样品质量评估可用于合理的液化评估,并且有可能使用重构样品,其小应变剪切模量与原位值相同,代替高质量的样品。 (C)2016年日本岩土学会。 Elsevier B.V.的制作和托管

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