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首页> 外文期刊>Journal of Petroleum Technology >Underbalanced Coiled-Tubing-Drilled Horizontal Well in the North Sea
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Underbalanced Coiled-Tubing-Drilled Horizontal Well in the North Sea

机译:北海欠平衡的连续油管钻井水平井

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摘要

Maersk Olie & Gas A/S (Maersk Oil) has drilled a 3,309-ft-long near-horizontal drainhole with coiled tubing to a total measured depth (MD) of 11,000 ft in the Danish sector of the North Sea. The well was completed in May 1994 as a 3(1/2)-in. openhole producer in the Gorm field chalk reservoir. Part of the well was drilled at underba-lanced conditions, and oil production rates of up to 1,100 STB/D were reached during drilling. Conventional well-test equipment was used for handling returns. A nearby process facilities platform supplied lift gas and received the produced hydrocarbons during the drilling phase. Worth noting are the penetration of several chert layers, the fairly long reach, and the application of geosteering. Indications were that the well productivity was significantly improved compared with that of a conventionally drilled well, but problems were experienced with borehole stability in a fractured region.
机译:马士基石油化工公司(Maersk Olie&Gas A / S)(马士基石油公司(Maersk Oil))在北海丹麦段钻了一个3,309英尺长的近水平排水孔,带有连续油管,总测量深度(MD)为11,000 ft。该井于1994年5月以3(1/2)英寸完工。 Gorm油田白垩储层中的裸眼生产商。该井的一部分是在欠平衡条件下进行钻探的,在钻探过程中产油率高达1100 STB / D。使用常规的经过良好测试的设备来处理退货。附近的加工设施平台在钻井阶段提供了提升气并接收了产生的碳氢化合物。值得注意的是几层of石层的渗透,相当长的覆盖范围以及地质导向的应用。有迹象表明,与常规钻探井相比,该井的生产率有了显着提高,但是在裂缝区域的井眼稳定性却遇到了问题。

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