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MODEL TESTS OF HYDRAULIC PERFORMANCE OF PIT 6 DAM STILLING BASIN

机译:Pit 6大坝ST水盆地水力性能模型试验

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摘要

Pit 6 Dam, located on the Pit River in northern California, was constructed by Pacific Gas and Electric Company in San Francisco in l965 for hydroelectric power generation. The gross head of the hydro- electric installation is 48.5 m for a rated generating capacity of 89 MW. Flow over the ogee spillway is regulated by two radial gates, and it discharges into a 33.5-m-wide and l9.5-m-long stilling basin. Since completion of the dam, there have been chronic problems with the floor blocks, some of which were dislodged more than once. To elucidate the primary cause of floor block failures and develop a new type of block, a 1:28-scale undistorted hydraulic model was constructed, and direct measurements of the longitudinal and lateral components of the forces acting on the model floor blocks were taken using a load cell. Extremely large fluctuating loads acting on the existing blocks in the lateral direction were found to be the primary cause of the block failures. Triangular hollow blocks, which substantially reduce the lateral loads, were then developed using the model.
机译:Pit 6大坝位于加利福尼亚北部的Pit河上,由太平洋天然气和电力公司于1965年在旧金山建造,用于水力发电。水力发电设备的总水头为48.5 m,额定发电容量为89 MW。 ogee溢洪道上的水流由两个径向闸门调节,并排入33.5米宽和199.5米长的静水池。自大坝完工以来,楼板一直存在长期性问题,其中一些被搬迁不止一次。为了阐明地板砖失效的主要原因并开发一种新型的砖块,构建了1:28比例的未变形水力模型,并使用以下方法直接测量了作用在模型地板砖上的力的纵向和横向分量称重传感器。发现在横向上作用在现有砌块上的波动很大,是造成砌块故障的主要原因。然后使用该模型开发了可大大减少侧向载荷的三角形空心块。

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