首页> 外文期刊>The Journal of Canadian Petroleum Technology >Study and Application of Gelled Foam for In-Depth Water Shutoff in a Fractured Oil Reservoir
【24h】

Study and Application of Gelled Foam for In-Depth Water Shutoff in a Fractured Oil Reservoir

机译:裂缝性油藏深度堵水胶凝泡沫的研究与应用

获取原文
获取原文并翻译 | 示例
           

摘要

A gelled foam is comprised of water, a foaming agent (surfactant), a foaming stabilizer (polymer) and a cross-linking agent. This system with gel as the outer phase is more stable than conventional foam that uses water as the outer phase. Therefore, the gelled foam system prolongs the effective period of water shutoff. By using the Ross Foamer Device to determine its foaming and stability characters, we verify that the best foaming agent is 0.3% YG240; the stable foam agent is 0.2 - 0.4% HP AM; the cross-linking agent is 0.09% sodium dichromate and 0.16% sodium sulphite and nitrogen. On the basis of bench-scale evaluations of characters on gelation time and water shutoff efficiency, the pilot test is performed on Well H1340 in the Huoshaoshan fractured reservoir. The workover program includes washing the larger fissures using a highly efficient oil displacement agent, injecting gelled foaming agent, over-displacing fluids, nitrogen and water, then shutting in the well for hardening. Field tests show that good blocking efficiency is gained in the well with a water cut decrease of 20 - 50% and oil production increase of 3.7 - 11.0 m~3/day.
机译:凝胶泡沫由水,发泡剂(表面活性剂),发泡稳定剂(聚合物)和交联剂组成。与以水为外相的常规泡沫相比,这种以凝胶为外相的体系更稳定。因此,凝胶泡沫系统延长了断水的有效期。通过使用Ross Foamer设备确定其起泡性和稳定性,我们验证了最佳起泡剂是0.3%的YG240。稳定的发泡剂为0.2-0.4%HP AM;交联剂为0.09%重铬酸钠和0.16%亚硫酸钠和氮气。在对胶凝时间和堵水效率等特征进行台规模评价的基础上,对霍韶山裂缝性油藏H1340井进行了中试。修井程序包括使用高效的驱油剂清洗较大的裂缝,注入胶凝的发泡剂,过量置换的流体,氮气和水,然后关闭井中进行硬化。现场测试表明,该井获得了良好的堵漏效率,含水率降低了20-50%,石油产量提高了3.7-11.0 m〜3 / day。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号