首页> 外文期刊>Journal of bridge engineering >Investigation of Distortion-Induced Web-Gap Cracking in a Seismically Retrofitted Steel Bridge: Repair Measures
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Investigation of Distortion-Induced Web-Gap Cracking in a Seismically Retrofitted Steel Bridge: Repair Measures

机译:钢筋混凝土桥变形引起的腹板裂缝的研究:修复措施

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This paper studies distortion-induced fatigue cracks in a 1960s-era welded plate girder bridge that developed cracks in the web-gap region shortly after completion of a comprehensive seismic retrofit. Finite-element analysis (FEA) and field testing were conducted to investigate the cause of cracking and then to recommend appropriate repair measures for the bridge. The field test results validated the high-stress concentrations in the web-gap region of the bridge that led to fatigue cracking after only a limited number of cycles. FEA results indicated that the high-stress concentrations were principally a result of replacing K-type diaphragms with stiffer cross diaphragms as part of the seismic retrofit. Two conventional repair measures in addition to two innovative repair measures were evaluated. The proposed innovative repair measures focused on ease of installation compared with more conventional options and were found to reduce the distortion-induced stresses well below the constant amplitude fatigue threshold (CAFT). (C) 2016 American Society of Civil Engineers.
机译:本文研究了在1960年代的焊接钢板箱梁桥中由变形引起的疲劳裂纹,该桥在全面的地震改造完成后不久在腹板间隙区域产生了裂纹。进行了有限元分析(FEA)和现场测试,以调查开裂的原因,然后为桥梁推荐适当的维修措施。现场测试结果验证了桥梁的腹板间隙区域中的高应力集中,仅在有限次数的循环之后就导致了疲劳裂纹。有限元分析结果表明,高应力集中主要是由于将K型膜片换成较硬的横向膜片作为地震改造的一部分。除了两个创新的维修措施外,还评估了两个常规的维修措施。与更常规的选择相比,所提出的创新性修复措施侧重于易于安装,并且发现该方法可将变形引起的应力降低到远低于恒定振幅疲劳阈值(CAFT)的水平。 (C)2016年美国土木工程师学会。

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