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Failure of a geomembrane lined embankment dam - Case study

机译:土工膜衬砌堤坝的破坏-案例研究

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The right wing embankment of the headrace channel of a hydropower plant, failed adjacent to the concrete intake structure. The failure also caused damages of the penstocks and flooding of the powerhouse. The root-cause analysis showed that water from the reservoir entered, through an open joint in the adjacent concrete structure, the geomembrane lined homogeneous embankment dam fill. This seepage water had eroded dam material from below the geomembrane and transported it to the drainage zones located at the interface of the embankment and concrete structures. Due to continuing seepage and erosion of dam material the geomembrane ruptured and this resulted in the full reservoir head being applied to the embankment fill material. This increased the seepage through the dam fill and caused concentrated leak erosion of the fine-grained material at the contact with the concrete structure, and this lead to the failure of the embankment.
机译:水电站头水渠右翼路堤在混凝土进水口结构附近失效。该故障还造成压力管损坏和动力装置泛滥。根本原因分析表明,来自水库的水通过相邻混凝土结构中的开口缝进入了衬有土工膜的均质路堤坝。渗水从土工膜下方侵蚀了坝体材料,并将其输送到路堤和混凝土结构界面处的排水区。由于坝体材料的持续渗漏和侵蚀,土工膜破裂,这导致整个储层顶部被应用到路堤填充材料上。这增加了通过大坝填充物的渗漏,并导致细粒材料在与混凝土结构接触时发生集中的泄漏侵蚀,并导致路堤的破坏。

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