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Reducing scrap and improving an air conditioning pipe production line

机译:减少废料并改善空调管生产线

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The automotive industry is considered one of the most demanding and competitive sectors in the global market. This increasingly implies having a stable and optimized production process, always with a view to continuous improvement. Therefore, it is very important to be aware of all the waste that is generated in all production and logistics operations and take action to reduce them. In this regard and considering the process of producing air conditioning pipes for the automotive industry, a high scrap value was detected mainly due to soldering process. Therefore, the entire production process is analyzed in order to identify the main causes behind the high scrap value. Several Lean and quality tools are used to reduce not only the amount of scrap but also to increase the line productivity. In order to face this challenge, after elaborating the action plan and corresponding implementation, the scrap value is reduced by 12% in general, and productivity increased by 29%, 55% and 22.5% in three different references produced by the same machine. Although this solution is a bit expensive, the corresponding payback is reduced, so it can easily be applied transversally to other similar machines allowing extremely interesting gains in the short term.
机译:汽车行业被认为是全球市场中最苛刻和最具竞争力的行业之一。这一越来越多地意味着具有稳定和优化的生产过程,始终以持续改进为视角。因此,了解在所有生产和物流运营中产生的所有废物非常重要,并采取行动减少它们。在这方面,考虑到为汽车工业生产空调管道的过程,主要由于焊接过程而检测到高废料值。因此,分析了整个生产过程,以识别高废料值背后的主要原因。几种精益和质量工具用于不仅可以减少废料量,而且还用于增加线生产力。为了面对这一挑战,在阐述行动计划和相应的实施方面,废钢值一般减少12%,在同一台机器生产的三种不同的参考文献中,生产率增加了29%,55%和22.5%。虽然该解决方案有点昂贵,但相应的回报减少,因此可以很容易地横向地应用于其他类似机器,允许短期内极其有趣的收益。

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