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Quality Control of the Steel Wire Rod Product by Integration Lean Six Sigma and Taguchi Method

机译:集成精益6西格玛和田口法的线材产品质量控制。

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摘要

RMW Inc. is the global company in Indonesia. One of its product is the steel wire rod. This research aims to control the production process and improve the product quality. This research is using the integration between lean six sigma and taguchi method. The first step is to reduce the waste using lean six sigma method while the second step is to reduce the defect using taguchi method. Based on the identification of seven waste, the most dominant waste is the defect that is caused by there is no setting of the roll entry guide. The product has 11 CTQ (critical to quality) with the focus on laps defect, underfill defect, and overfill defect. Then, the cause of failure is identified using FMEA (failure mode effect analysis). The level of sigma capability is achieved at 4.54 with DPMO (defect per million opportunities) is 4006.55. The first improvement can reduce the time until 8.9 minutes. The second improvement sets the roll entry guide. The optimum factors for setting of the roll entry guide is A factor with 150 tonnages of wear level, C factor by 5 bar of cooling and D factor by 6 ml of lubrication.
机译:RMW Inc.是印度尼西亚的全球公司。其产品之一是钢丝。这项研究旨在控制生产过程并提高产品质量。这项研究是利用瘦六西格玛和塔古奇方法之间的集成。第一步是使用瘦六西格玛方法减少浪费,而第二步是使用塔古奇方法减少缺陷。根据对七种废料的识别,最主要的废料是由于未设置卷筒进纸导轨而导致的缺陷。该产品具有11个CTQ(对质量至关重要),重点在于搭接缺陷,底部填充缺陷和过量填充缺陷。然后,使用FMEA(故障模式影响分析)确定故障原因。 DPMO(每百万机会的缺陷数)为4006.55时,sigma功能级别达到4.54。第一次改进可以将时间减少到8.9分钟。第二项改进设置了卷入指南。设置辊子入口导板的最佳因素是A因子,其磨损量为150吨,C因子为5 bar冷却,D因子为6 ml润滑。

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