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Pretreatment of Process Condensate with Ammonia Degassing in CAN Fertilizer Production

机译:CAN肥料生产中氨气脱气对工艺冷凝液的预处理

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In the production process of calcium ammonium nitrate (CAN) fertilizer, process-condensate isgenerated with a high content of ammonium nitrogen. Such high mass concentration of ammoniumnitrogen (approximately 2 g L–1) significantly burdens the operation of the wastewater treatmentplant, where the process condensate is treated by method of ion exchange. At CAN 1 Plant,a degassing system for process condensate was built. After pretreatment, the concentration ofammonium nitrogen in the process condensate was reduced to less than 500 mg L–1.Before upgrading with degassing system, the process condensate from CAN 1 Plant was collectedin tank TK 17 301, from which it was pumped to the wastewater treatment plant to be treated bythe method of ion exchange. When CAN 1 Plant is in normal operation, 10 m3h–1 of process condensateis formed with pH around 10, and temperatures around 50 °C. The degassing system ofprocess condensate consists of a new tank, TK 17 504, which is connected with new pipeline tothe tank TK 17 301. The process condensate input was transferred from the old to the new tank,TK 17 504. A new pump was installed for regulation of process condensate and bursting abovethe condensate level.Additional stimulation for ammonia degassing followed, after the return of 12 bar steam condensateinto the tank TK 17 504. Consequently, the process condensate temperature increasedto 80 C. Degassed ammonia is introduced into the existing system for washing gases and returnsinto the process of fertilizer production.By degassing ammonia from the process condensate at CAN 1 Plant, 10.7 kg h–1 of ammonia returnsinto the fertilizer production process.Additionally, there has been an improved performance of the wastewater treatment plant, so thatin December 2010, the volume of treated wastewater was almost 80 000 m3 which is an increaseof 86 %.
机译:在硝酸铵钙(CAN)肥料的生产过程中,会生成高氨氮含量的过程冷凝物。如此高的氨氮浓度(约2 g L–1)显着加重了废水处理厂的运行,废水处理厂通过离子交换方法处理过程中的冷凝水。在CAN 1工厂,建立了用于过程冷凝物的脱气系统。经过预处理后,过程冷凝物中的氨氮浓度降至500 mg L-1以下。在进行脱气系统升级之前,将来自CAN 1工厂的过程冷凝物收集到TK 17 301储罐中,然后将其泵入废水中。用离子交换法处理的污水处理厂。当CAN 1工厂处于正常运行状态时,会形成10 m3h–1的过程冷凝物,pH约为10,温度约为50°C。过程冷凝物的脱气系统由一个新的储罐TK 17 504组成,该储罐与新管道连接到该储罐TK 17301。过程冷凝物的输入从旧的储罐转移到新的储罐TK 17 504。将12 bar的蒸汽冷凝水返回罐TK 17504后,对氨进行脱气的其他刺激措施。因此,过程冷凝水的温度升至80°C。将脱气的氨引入现有系统中通过将CAN 1工厂的过程冷凝物中的氨脱气,将10.7 kg h-1的氨返回到肥料生产过程中。此外,废水处理厂的性能得到了改善,到2010年12月,处理后的废水量接近8万立方米,增长了86%。

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