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Dry re-forming of methane to synthesis gas over lignite semicokes catalyst at high pressure

机译:在高压下通过褐煤半焦催化剂将甲烷干重整为合成气

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Dry re-forming of methane has been carried out in a high temperature-pressure reactor at different pressures, using Hongce lignite semicokes catalyst. The results show that CH"4 and CO"2 conversions are decreased as the reaction pressure increased, but both of them kept basically stable when the reaction pressure is between 0.3 and 1 MPa. The comparison shows that the effects of the temperature and the flow of reactant gas on dry re-forming of methane are consistent with between high pressure and atmospheric pressure. The ratio of CO/H"2 decreased as the ratio of CH"4/CO"2 increased, yet the value of CO/H"2 is always more than 1 at different pressures. Hongce lignite semicokes catalyst is characterized by FTIR, XRD, SEM and BET, and the analysis results reveled that the physical specific adsorption peak of CO"2 at 2350 cm^-^1 is strengthened significantly at different pressures, the micropore area and volume of Hongce lignite semicokes reduced form 40.2 m^2 g^-^1 and 0.019 cm^3 g^-^1 to 34.9 m^2 g^-^1 and 0.017 cm^3 g^-^1, respectively. Hongce lignite semicokes catalyst exhibited better activity and stability within 0.3-1 MPa range.
机译:使用Hongce褐煤半焦催化剂,在高温高压反应器中,在不同压力下进行了甲烷的干重整。结果表明,随着反应压力的增加,CH” 4和CO” 2的转化率降低,但当反应压力在0.3和1 MPa之间时,两者基本保持稳定。比较表明,温度和反应气体流量对甲烷干重整的影响与高压和大气压之间是一致的。随着CH” 4 / CO” 2的比例增加,CO / H” 2的比例降低,但在不同压力下,CO / H” 2的值始终大于1。用FTIR,XRD,SEM和BET等方法对红炭褐煤半焦催化剂进行了表征,分析结果表明,在不同压力,微孔面积和体积下,CO 2在2350 cm ^-^ 1处的物理比吸附峰明显增强。洪斯褐煤半焦分别从40.2 m ^ 2 g ^-^ 1和0.019 cm ^ 3 g ^-^ 1减少到34.9 m ^ 2 g ^-^ 1和0.017 cm ^ 3 g ^-^ 1。催化剂在0.3-1 MPa范围内表现出更好的活性和稳定性。

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