首页> 外文期刊>International Journal of Oil, Gas and Coal Engineering >Research and Application of Micronized Barite Drilling Fluid in HPHT Wells of the Western South China Sea
【24h】

Research and Application of Micronized Barite Drilling Fluid in HPHT Wells of the Western South China Sea

机译:南海西部HPHT井超细重晶石钻探液的研究与应用

获取原文
           

摘要

When drilling wells in high temperature and high pressure (HTHP) fields, the drilling fluid properties are of utmost importance. If the viscosity of high density drilling fluid is too low, it will lead to barite sag and poor cuttings carrying capacity. However, lost circulation will occur due to high surge pressure and Equivalent Circulating Density (ECD) caused by high viscosity. High density drilling fluid performance is largely dependent on the use of the weighting material. The contradiction between rheological properties and barite sag of API Barite High Density Drilling Fluid (HABF) is great in the condition of HTHP. This article describes a novel weighting material that has resulted in a ten-fold reduction in the particle size of API barite. With this micronized barite, the contradiction of high density drilling fluid can be solved. The rheology, sag stability and lubricity of high density drilling fluid weighted by micronized barite and API barite is investigated in the laboratory. And the mechanism of micronized barite to improve the performance of high density drilling fluid is discussed by using size distribution, surface charge, and microscopic shape method. Micronized Barite High Density Drilling fluid (HMBF) was first applied in two HTHP exploration wells with good gas show recently, which are in Western South China Sea. HMBF exhibited good rheological properties, sag stability and lubricity in the drilling process. Drilling task was successfully completed, without complicated situation.
机译:在高温高压(HTHP)领域中钻井时,钻井液的特性至关重要。如果高密度钻井液的粘度太低,将导致重晶石下陷和较差的钻屑承载能力。但是,由于高浪涌压力和高粘度导致的等效循环密度(ECD)会导致漏液。高密度钻井液的性能很大程度上取决于配重材料的使用。在高温高压条件下,API重晶石高密度钻井液(HABF)的流变性能与重晶石下垂之间存在很大的矛盾。本文介绍了一种新型的加重材料,该材料已使API重晶石的粒度降低了十倍。使用这种微粉状的重晶石,可以解决高密度钻井液的矛盾。在实验室研究了由微粉状重晶石和API重晶石配重的高密度钻井液的流变性,流挂稳定性和润滑性。通过尺寸分布,表面电荷和微观形貌方法探讨了微晶重晶石改善高密度钻井液性能的机理。微粉化重晶石高密度钻井液(HMBF)首次在南海西部的两个高温气密性良好的HTHP勘探井中应用。 HMBF在钻井过程中表现出良好的流变性,下垂稳定性和润滑性。钻井任务顺利完成,情况不复杂。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号