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Resolving serious seepage through karstified limestone at the Mujib Dam, Jordan

机译:解决约旦穆吉布水坝的喀斯特石灰岩渗漏问题

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The 67 m high Mujib Dam (Jordan) was built between 1999 and 2003 in Cretaceous limestone with intercalated marls in the middle of the section. Initial investigations indicated only moderate permeability, hence prior to impoundment a normal grouting program was undertaken extending to 50 m in depth. Initially, little seepage was observed when the lower section of the reservoir was filled. After a dry summer, heavy rainfall filled the reservoir overnight to its maximum water level (194 m a.s.l.). A sudden seepage began downstream of the right abutment, which reached 140 1/s by morning, increasing to up to 240 1/s during the following 2 weeks. Although a second grouting program reduced the seepage to some 3 1/s of highly mineralized water, there were concerns as to the adequacy of the Phase 1 grouting. A detailed analysis of the testing and grouting results indicated that the hydraulic pressures created by the sudden increase of water in the reservoir had washed out the natural infill which had previously sealed karstic voids.
机译:高67 m的Mujib大坝(约旦)建于1999年至2003年之间,位于白垩纪石灰岩中,中间夹有泥灰岩。初步研究表明,渗透率只有中等水平,因此在蓄水之前,要进行常规的注浆程序,扩展到深度50 m。最初,当储层下部充满时,几乎没有渗漏。夏季干燥后,暴雨使水库过夜,直至达到最高水位(194 m a.s.l.)。右基台的下游开始突然渗水,到早晨达到140 1 / s,在接下来的2周内增加到240 1 / s。尽管第二次灌浆计划将渗漏减少到高度矿化水的约3 1 / s,但仍对第一阶段灌浆的适当性表示担忧。对测试和灌浆结果的详细分析表明,由储层中水的突然增加所产生的水压已冲走了天然填充物,而天然填充物以前已经密封了岩溶空隙。

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