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Modification of an Industrial Ethane Recovery Plant Using Mixed Integer Optimization and Shuffled Frog Leaping Algorithm

机译:混合整数优化和改组蛙跳算法对工业乙烷回收厂的改造

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摘要

A currently in operation ethane recovery plant was simulated and compared with the real one. The objective of this process is to separate C_1-C_2 and C_3~+ at the minimum utility cost. Then, optimal operating parameters were determined, in which the objective function is based on the plant profit. Shuffled frog leaping algorithm was applied for the optimization of this plant. The algorithm parameters were adjusted for improving the performance of the algorithm through optimization of the problem. The results show that at the optimum point the profit increased by 2.4 % and utility costs decreased by 5 %. In the next part, the potential of the plant for modification of the process configuration was considered. The analysis showed that it is possible to improve the process and refrigeration cycle configurations to the more efficient one. In the optimum point the profit increased by 8 % towards the base case and operating cost decreased by 12.8%.
机译:模拟了目前正在运行的乙烷回收装置,并将其与实际装置进行了比较。此过程的目标是以最小的使用成本分离C_1-C_2和C_3〜+。然后,确定最佳运行参数,其中目标函数基于工厂利润。应用改组蛙跳算法对该植物进行了优化。调整算法参数以通过优化问题来提高算法性能。结果表明,在最佳点,利润增加了2.4%,公用事业成本减少了5%。在下一部分中,将考虑工厂对流程配置进行修改的潜力。分析表明,可以将过程和制冷循环配置改进为更有效的配置。在最佳点上,基本情况的利润增加了8%,运营成本减少了12.8%。

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