首页> 外文会议>Water Environment Federation 72nd annual conference amp; exposition (WEFTEC'99) >EVALUATION, IMPLEMENTATION, AND OPTIMIZATION OF LOW-LEVEL ARSENIC REMOVAL TECHNOLOGIES FOR A GROUNDWATER REMEDIATION SYSTEM
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EVALUATION, IMPLEMENTATION, AND OPTIMIZATION OF LOW-LEVEL ARSENIC REMOVAL TECHNOLOGIES FOR A GROUNDWATER REMEDIATION SYSTEM

机译:地下水修复系统中低水平除砷技术的评估,实施和优化

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This paper documents laboratory testing, field scale pilot testing, and full scalernimplementation activities for removal of low level arsenic in a groundwater remediationrnapplication. Groundwater contamination, primarily xylenes, existed as a result ofrnprevious operations at the facility. In order to minimize seepage of contaminatedrngroundwater into an adjacent drainage canal, a groundwater recovery and treatmentrnsystem (GRTS) was installed in early 1996. The GRTS consisted of three extractionrnwells with dedicated submersible pumps, an air stripper, carbon polishing, and on-siterndisposal of the treated groundwater. An Air Sparging/ Soil Vapor Extraction Systemrn(AS/SVE) was subsequently installed to efficiently address source removal upgradientrnof the GRTS extraction system.rnThe GRTS satisfactorily treated the ground water to Florida Department ofrnEnvironmental Protection (FDEP) standards for volatiles. However, during the initialrnmonths of operation, the extracted groundwater consistently contained arsenic atrnlevels exceeding the primary drinking water standard (50 ug/L). Arsenic levels in thernextracted groundwater ranged from 61 to 137 ug/L with an average of 101 ug/L. Thernsource of arsenic appears to be isolated in a small area near the wells and wasrnunexpected, considering that arsenic was not historically used in quantities at thernplant. Due to the consistency and level of detection, FDEP required that arsenic bernremoved to below 50 ug/l prior to on-site discharge.rnAlthough precipitation is commonly used to remove arsenic from aqueous wasternstreams, concerns over the effectiveness of achieving removal to ppb levels andrnsludge handling issues resulted in the evaluation of other technologies. In order tornscreen alternative technologies, bench scale treatability studies were conducted usingrnthe following treatment approaches: 1) Lignite Granular Activated Carbon (LGAC); 2)rnTreated Granular Activated Carbon (TGAC); 3) Activated Alumina (AA); 4) IonrnExchange (IX); and 5) Ozone.rnBased upon the results of the bench scale testing , the following were determined tornbe potentially feasible: activated alumina, iron impregnated carbon, and ion exchange.rnEach of these three technologies were then subjected to a screening level analysisrnbased upon effectiveness, and costs for both long and short term operation. Basedrnupon this screening level evaluation, it was determined that ion exchange offered arnfeasible technology with the greatest flexibility for implementation..rnIt was also decided that a flow through rather than batch test of an ozone assistedrnfiltration technology should be further tested. This test can be easily accomplishedrnand has the potential to offer substantial benefit.rnUpon completion of the two field scale pilot tests, ion exchange was selected forrnarsenic removal. The key factors influencing this decision were low capital cost andrnreliability of the resin. The full scale system was installed consisting of two canistersrnoperating in series in March 1998.rnThe full scale resin system has now been operational for over 6 months with the fullrnscale system demonstrating arsenic removal to ppb levels thus achieving designrngoals.. During this time, however resin bed life at full scale operation was variable.rnThis was identified by observance of normal resin life in the first canister followed byrnrapid exhaustion of a second canister when moved to the lead position. Additional pHrnand arsenic monitoring were implemented to characterize system behavior. The resultsrnsupport the probable cause of apparent anion fouling. A key finding in the systemrnoperations review was that the capacity of the second canister to remove arsenic wasrnbeing exhausted at nearly the same rate of the first canister . It is suspected that thernarsenic removal front (break through point) is lagging the "fouling anion" front therebyrnresulting in the reduction of arsenic capacity during the latter stages of canisterrnoperation. Samples are currently being analyzed to confirm carbonate and otherrnanion fouling of these resins. However, operational adjustments have been made inrnthe interim to counteract the affects of this fouling and maintain successful operationrnof the resin system.rnThis abstract summarizes the testing and evaluation (technical and cost effectiveness)rnthat was completed for this project. The paper will present the specific detail of therntechnical data that was collected and its impact on cost analysis decisions that werernmade. The paper is also important in documenting the real-world process of testing,rnevaluation and full scale implementation from identification of the problem throughrnbench scale testing, field pilot testing, full scale implementation, and operationalrnadjustments necessary to assure continued satisfactory performance.
机译:本文记录了用于地下水修复应用中的低水平砷去除的实验室测试,现场规模的中试测试和全面实施活动。工厂先前的作业导致地下水污染,主要是二甲苯。为了最大程度地减少被污染的地下水渗入相邻的排水渠,1996年初安装了地下水回收和处理系统(GRTS)。GRTS由三个抽水井组成,这些抽水井配有专用的潜水泵,空气汽提器,碳抛光和对废水的即时处置。处理过的地下水。随后安装了空气喷射/土壤蒸汽提取系统(AS / SVE),以有效解决GRTS提取系统对源去除的升级。但是,在运行的最初几个月中,提取的地下水始终含有超过主要饮用水标准(50 ug / L)的砷。提取的地下水中的砷含量范围为61至137 ug / L,平均为101 ug / L。砷的来源似乎是在井附近的一个小区域中隔离的,并且是意外的,这是因为从历史上讲,工厂没有大量使用砷。由于检测的一致性和水平,FDEP要求在现场排放之前将砷去除至50 ug / l以下。尽管通常使用沉淀法从水流中去除砷,但对于将其去除至ppb水平和去除污泥的有效性存在担忧处理问题导致对其他技术的评估。为了撕裂替代技术,使用以下处理方法进行了台式可处理性研究:1)褐煤颗粒活性炭(LGAC); 2)rnt颗粒活性炭(TGAC); 3)活性氧化铝(AA); 4)IonrnExchange(IX); 5)臭氧。根据工作台规模测试的结果,确定了以下可能可行的方法:活性氧化铝,铁浸渍的碳和离子交换。然后,根据有效性对这三种技术分别进行筛选水平分析,以及长期和短期运营的成本。基于此筛选水平评估,确定了离子交换技术为实施提供了最大的灵活性。.还决定应进一步测试臭氧辅助过滤技术的流通而不是分批测试。该测试很容易完成,并有可能带来实质性的好处。在完成两个现场规模的中试测试后,选择了离子交换技术来去除砷。影响这一决定的关键因素是较低的投资成本和树脂的可靠性。完整规模的系统于1998年3月安装,由两个串联的碳罐组成。rn完整规模的树脂系统现已运行了6个月以上,该完整规模的系统表明砷的去除量达到ppb级别,从而达到了设计目标。全尺寸操作的床寿命是可变的。这可以通过观察第一个滤罐中正常的树脂寿命来确定,然后移动到领先位置时第二个滤罐会迅速耗尽。实施了附加的pHrn和砷监测以表征系统行为。结果支持了明显的阴离子结垢的可能原因。在系统操作审查中的一个关键发现是第二罐清除砷的能力几乎与第一罐相同。怀疑脱砷前沿(突破点)落后于“结垢阴离子”前沿,从而导致在罐操作的后期阶段砷容量的降低。目前正在对样品进行分析,以确认这些树脂的碳酸盐和其他硫杂垢。但是,在过渡期间已进行了操作调整,以抵消这种结垢的影响并维持树脂系统的成功运行。本摘要总结了为该项目完成的测试和评估(技术和成本效益)。本文将详细介绍所收集的技术数据及其对制定的成本分析决策的影响。该文件对于记录现实世界中的测试,重新评估和全面实施过程也很重要,这可以通过基准规模测试,现场先导测试,全面实施以及为确保持续令人满意的性能所必需的操作调整来确定问题。

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