首页> 外文会议>Sugar Processing Research Conference; 20020310-20020313; New Orleans,LA; US >FURTHER INSIGHTS ON THE FACTORY PERFORMANCE OF COLD, INTERMEDIATE, AND HOT LIME CLARIFICATION SYSTEMS
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FURTHER INSIGHTS ON THE FACTORY PERFORMANCE OF COLD, INTERMEDIATE, AND HOT LIME CLARIFICATION SYSTEMS

机译:对冷,中,热石灰澄清系统出厂性能的进一步了解

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Since 1996, Cora Texas factory in Louisiana has been operating intermediate lime clarification and was, therefore, one of the few U.S. factories that did not operate cold lime clarification. In an attempt to further improve clarification performance, the factory made the decision to convert to hot lime clarification during the 2000 grinding season. A comparative investigation of hot versus intermediate and cold lime clarification was undertaken to quantify performance. In cold liming, mixed juice (MJ) was incubated (8min) and then limed in a lime tank (4min), both at ~105℉. For intermediate liming, 50% of the MJ was heated (180-200℉) before incubation (8min), then limed in a lime tank (4min) at~150℉. Hot liming was configured very similar to intermediate liming except that incubation time was increased from 8 to 12 mins, and that lime was added immediately after flash-heating (215℉; 30sec). Hourly samples across each of the three processes were collected over a six hour sampling period, on three consecutive days respectively, and these were repeated three times across the 2000 grinding season. For most clarification parameters investigated, both hot and intermediate liming performed much better than cold liming, and hot liming generally offered some extra advantages over intermediate liming. Less sucrose was lost to inversion reactions across both hot (season av. 0.79%) and intermediate (0.97%) lime processes than across cold liming (1.48%). By operating hot liming, the reduction in sucrose losses alone saved the factory approximately US$283,000 over cold liming. Increasing the factory target pH of the final evaporator syrup (FES) from ~pH 6.0 to 6.3, in sampling period 3 in both hot and intermediate liming, caused a very marked reduction in sucrose inversion losses, particularly across the clarifiers and evaporators. Dramatically less lime had to be added in hot liming compared to either cold or intermediate liming, with the factory consuming, on season average, only 1.01 Ibs lime/ton cane compared to 1.28 for the 1999 grinding season when intermediate rather than hot liming was operated. Pre-heating 50% of the MJ in both intermediate and hot liming consistently removed color, dextran, and starch, but silicate levels were not significantly changed. Although, the fastest settling occurred in intermediate liming, ~ 2.1% (season av.) more turbidity removal (MJ to clarified juice [CJ]) occurred hi both hot and intermediate liming compared to cold liming, with better CJ turbidity control. Subsequent FES and raw sugar turbidity values were better in hot liming. Markedly less color (~2.5%) formed on hot liming because of reduced retention time of liming, compared to ~17% color formation in cold and intermediate lime clarification. Dextran removal was best across hot liming and, as expected, dextran formed in the cold lime tanks. Using hot liming across the season, the factory observed 12-15% more heating capacity in the limed juice heat exchangers and a 90% reduction in the quantity of chemicals needed to clean the heat exchangers.
机译:自1996年以来,位于路易斯安那州的Cora Texas工厂一直在进行中间石灰澄清,因此是美国少数几家未进行冷石灰澄清的工厂之一。为了进一步提高澄清性能,工厂决定在2000年的研磨季节转换为热石灰澄清。进行了热石灰,中石灰和冷石灰澄清度的对比研究,以量化性能。在冷石灰中,将混合汁(MJ)保温(8分钟),然后在石灰罐中撒石灰(4min),两者均在〜105℉下进行。对于中间石灰,在孵化前(8min)加热50%的MJ(180-200180),然后在约150℉的石灰罐中撒石灰(4min)。除了将保温时间从8分钟增加到12分钟,并且在快速加热(215秒; 30秒)后立即添加石灰外,热石灰的配置与中间石灰非常相似。在六个小时的采样期内,分别连续三天收集三个过程中每个过程的每小时样本,并在2000研磨季节中重复三次。对于所研究的大多数澄清参数,热和中间石灰的性能都比冷石灰好得多,而且热石灰通常比中间石灰具有一些额外的优势。与冷石灰(1.48%)相比,热石灰(季节平均0.79%)和中间石灰工艺(0.97%)的转化反应损失的蔗糖更少。通过使用热石灰,仅蔗糖损失的减少就比冷石灰为工厂节省了约283,000美元。在热和中灰过程中的采样期3中,将最终蒸发器糖浆(FES)的工厂目标pH从〜pH 6.0增加到6.3,从而使蔗糖转化损失显着降低,尤其是在澄清池和蒸发器中。与冷或中型石灰相比,热型石灰中添加的石灰少得多,工厂平均每季只消耗1.01 lbs石灰/吨甘蔗,而在1999年的研磨季节中,使用中型而不是热型石灰时,平均消耗量为1.28 lbs。 。在中间和热石灰中预热50%的MJ可以持续去除颜色,右旋糖酐和淀粉,但硅酸盐的含量没有明显变化。尽管在中温石灰中沉降最快,但在冷热石灰中和中温石灰中,除浊(MJ到澄清果汁[CJ])的浊度去除率均达到〜2.1%(季节平均值),CJ浊度控制效果更好。随后的FES和原糖浊度值在热石灰中更好。与减少的石灰留着时间相比,在热石灰上形成的颜色明显减少(约2.5%),而在冷石灰和中等石灰澄清中形成的颜色只有约17%。葡聚糖的去除最好在热石灰中进行,并且正如预期的那样,在冷石灰储罐中形成的葡聚糖。在整个季节中使用热石灰,工厂观察到榨汁热交换器的热容量增加了12-15%,清洁热交换器所需的化学物质数量减少了90%。

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