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Analysing and Rehabilitating Rock Mass Failure in Critical Mine Infrastructure

机译:分析和修复关键矿山基础设施中的岩体破坏

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摘要

To optimise the haulage of the large tonnages produced from stopes in this high production gold mine, an ore pass and feeder system was introduced. This ore pass was designed and developed in 2006 and the plate feeder installed and commissioned soon after. Cavity Monitoring Surveys (CMS) have been undertaken of the ore pass since it was commissioned. The original thickness that was surveyed of the pillar between the ore pass and decline in 2006 was approximated to be 19 m. Throughout its use large blocks of rock were reporting at the plate feeder. This was the first indication that the ore pass was failing somewhere between the tipping level of the 9410 level and the plate feeder at the 9330. Even so CMS surveys were not taken systematically to firstly identify the area of failure or for monitoring. In August 2008 after implementing management systems, large blocks were still reporting to the plate feeder. The decision was made to empty the pass enough to carry out a CMS survey of the area. Subsequently it was discovered that the area of failure was between the decline and ore pass and that since the first survey the pillar thickness had been reduced to approximately 9.7 m. Further management controls were put in place to slow movement of the material and to limit the use of the 9410 tipping level, but this did not alleviate the rate of failure entirely. The results of an initial inelastic numerical model indicated that most of the pillar was damaged and that failure into the decline likely if no changes were made. The numerical modelling predicted that even if material was no longer passing through the ore pass interaction between the voids was unavoidable and would most likely result in instability. The ore pass and plate feeder are an integral part of the haulage system for the remaining life-of-mnie. Two solutions were sought to firstly reinforce and stabilise the pillar between the ore pass and decline and secondly to rehabilitate the ore pass or find an alternate design that could still utilise the plate feeder. This paper summarises the analysis and resulting rehabilitation that was used to accomplish this.
机译:为了优化此高产金矿中采场产生的大吨位的运输,引入了矿石通行证和进料器系统。该矿石通道是在2006年设计和开发的,不久之后便安装并调试了平板给料机。自通行以来,就进行了空腔监测调查(CMS)。 2006年在矿石通过和下沉之间对支柱进行调查的原始厚度约为19 m。在整个使用过程中,在板式给料机上报告了大块岩石。这是第一个迹象表明矿石通过在9410的倾翻水平和9330的平板进料器之间失败。即使这样,CMS勘测也没有系统地进行以首先确定故障区域或进行监控。在实施管理系统后,2008年8月,大块仍在向印版进纸器报告。决定将通行证清空,以进行该区域的CMS调查。随后发现,破坏区域介于下降和矿石通过之间,并且自第一次测量以来,柱厚度已减小至约9.7 m。采取了进一步的管理控制措施,以减慢材料的移动速度并限制9410倾卸水平的使用,但这并不能完全缓解故障率。最初的非弹性数值模型的结果表明,大多数支柱都被损坏,并且如果不进行任何更改,很可能会失败而无法使用。数值模型预测,即使材料不再通过矿石,空洞之间的相互作用也是不可避免的,并且极有可能导致不稳定。矿石通行证和板式给料机是拖运系统不可或缺的一部分,可延长其使用寿命。寻求两种解决方案,首先是加固和稳定矿石通过和下降之间的支柱,其次是修复矿石通过或找到仍然可以使用板式给料机的替代设计。本文总结了用于完成此操作的分析和结果修复。

著录项

  • 来源
  • 会议地点 Sydney(AU)
  • 作者

    E Jones; RVarden;

  • 作者单位

    Senior Geotechnical Engineer, Yilgarn Shared Services, Barrick Gold Corporation, Level 4,200 Adelaide Terrace, Perth WA 6000;

    Senior Geotechnical Engineer, Kanowna Belle, Barrick Gold Corporation, P0 Box 1662, Kalgoorlie WA 6433;

  • 会议组织
  • 原文格式 PDF
  • 正文语种 eng
  • 中图分类 矿山开采;
  • 关键词

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