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PRECAST DOUBLE TEE ROOF COLLAPSE INVESTIGATION - A CASE STUDY

机译:预制双T形屋顶坍塌调查-案例研究

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During heavy rains in 2009, a portion of a concrete double tee (DT) roof system of an industrial building collapsed. Subsequently, an investigation ensued in order to determine the cause, and if other DT members were damaged. Remaining DT members with deflections between one and three-and-a-half inches, under dead loads, were discovered and the authors were tasked with determining the cause of the deflection as others had opined the deflections were due to long-term creep. This paper outlines the investigative process including historical loading events/collapse, weather research, and methodology used to determine the cause of the large deflections. Through investigation, it was determined that the collapse was due to significant rainfall that occurred in a short time, coupled with an inadequate roof drainage system and poor maintenance of roof drains. Calculations showed that the excessive deflections were not due to long-term creep but to a one time loading event that caused the permanent strain set in the DT strands. Although prestress/precast concrete structures are resilient, this case study highlights the importance of proper design and maintenance. Architects, engineers, building owners, and maintenance personnel can all learn lessons through this case study.
机译:在2009年的大雨期间,一栋工业建筑的混凝土双三通(DT)屋顶系统的一部分坍塌了。随后,进行了调查以确定原因,以及其他DT成员是否受损。发现了在静载作用下挠度在1-3英寸半英寸之间的其余DT构件,作者的任务是确定挠度的原因,其他人则认为挠度是由于长期蠕变引起的。本文概述了调查过程,包括历史荷载事件/倒塌,天气研究以及用于确定大变形原因的方法。通过调查,确定倒塌是由于短时间内大量降雨造成的,再加上屋顶排水系统不足和屋顶排水管维护不良。计算表明,过度的挠曲不是由于长期蠕变,而是由于一次加载事件导致了DT股中的永久应变。尽管预应力/预制混凝土结构具有弹性,但本案例研究突出了正确设计和维护的重要性。建筑师,工程师,建筑业主和维护人员都可以通过此案例研究来学习课程。

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