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PAPER MACHINE HOODS - BACK TO BASICS

机译:造纸机罩-返璞归真

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摘要

Historically low fuel costs, relatively high ambient temperatures and stable humidity in Queensland, and the luxury of a steam surplus meant the paper machine hood ventilation system at Visy Paper 8 was hardly a priority. However, a site wide energy audit suggested hood system inefficiencies were inflating steam usage by up to 3%. With energy prices rising, and the continuous push for increased paper production threatening the steam surplus, a project to optimise drying efficiency and reduce steam usage was quickly undertaken. This focus on the hood system promoted functional and operational understanding, but most importantly achieved the steam savings with minimal cost required. Investigations kicked off with benchmarking the system performance and operational practice. Measurements of supply and exhaust air flow, temperature and humidity data were compared to third party audits to develop process understanding and establish data confidence. It was also important to determine standard steam usage with constant paper grade and machine speed to justify project benefits. Data was collected across a range of paper grades and speeds to get a comprehensive picture of the hood dynamics under different operation conditions. With reasonable supply air temperatures and no major moisture leaks into the supply air, the opportunity at Visy Paper 8 lay in optimising air management across the hood. The issue lay in low supply air flow and misdirected exhaust air flow. Supply air was boosted by re-opening air distribution boxes and exhaust air was corrected by closing all doors, sealing up the hood and adjusting system ducting to capture air from across the whole hood. For minimal cost, this brought the balance between supply and exhaust air back into the design range for the enclosed-type hood. Steam usage was seen to drop by 2-3%, reducing our tonne of steam per tonne of paper requirements. Further higher cost opportunities exist, such as cleaning heat exchanger tubes and replacing steam traps but keeping control of the hood system basics is the first priority in promoting drying efficiency. This can be achieved with continual process data collection and analysis to prevent adopting an inefficient operating practice which will cost more in the long run.
机译:历史上较低的燃料成本,相对较高的环境温度和昆士兰州的稳定湿度,以及多余的蒸汽,这意味着Visy Paper 8的造纸机机罩通风系统几乎不是优先事项。但是,一次现场能源审计表明,抽油烟机系统效率低下,使蒸汽用量最多增加了3%。随着能源价格的上涨,以及不断增加的造纸产量的威胁,蒸汽过剩的威胁,迅速进行了优化干燥效率和减少蒸汽用量的项目。这种对引擎盖系统的关注促进了对功能和操作的理解,但最重要的是,以最低的成本实现了蒸汽节省。以基准测试系统性能和操作实践为起点的调查。将送风和排气流量,温度和湿度数据的测量结果与第三方审核进行比较,以了解过程并建立数据可信度。确定具有恒定纸张等级和机器速度的标准蒸汽用量也很重要,以证明项目收益的合理性。收集了各种纸张等级和速度的数据,以全面了解油烟机在不同操作条件下的动态。借助合理的送风温度,并且没有大量湿气泄漏到送风中,Visy Paper 8的机会在于优化整个机罩的空气管理。问题在于供气量低和排气流方向错误。通过重新打开空气分配箱来增强送风量,并通过关闭所有门,密封通风柜并调节系统管道来收集整个通风柜中的空气来纠正废气。为了使成本最小化,这使供气和排气之间的平衡回到了封闭式抽油烟机的设计范围。蒸汽使用量下降了2-3%,从而减少了每吨纸张所需的蒸汽量。还存在更高的成本机会,例如清洁热交换器管和更换蒸汽疏水阀,但保持通风柜系统基本知识的控制是提高干燥效率的首要任务。这可以通过持续的过程数据收集和分析来实现,以防止采用效率低下的操作方法,从长远来看,这将花费更多。

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