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Environmentally Sensitive Well Successfully Drills Underbalanced Using Recycling Technology

机译:环境敏感性良好地利用回收技术成功钻取不平衡

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In 2005 a sour underbalanced horizontal gas well was designed and drilled in a pristine, environmentally sensitive region of southern Alberta, Canada. There were two primary drivers for the client. One was to remain under reservoir pressure throughout drilling and completion operations and the second driver was to safely recover 9.0% hydrogen sulfide (H(2)S) gas production and recycle the H(2)S contaminated drilling fluid. The well was not classified as critical sour because of its proximity to populated areas and a low well productivity of 0.015 E(3)m(3)/kPa (0.37 Mscf/psi); however, a cumulative flaring limit of 240 E(3)m(3) (8.5 MMscf) was imposed by Alberta’s Energy and Utility Board (EUB). Casing and hole sizes were optimized after confirming the well could be successfully drilled underbalanced to total depth (TD). Both well engineering and process engineering were integrated to provide the process and equipment to accommodate the sour well effluent while controlling the downhole multiphase flow and pressure environment. The injection gas for the underbalanced section was supplied via on-site compression from a sales quality gas supply line at a rate of up to 55 sm3/min (1,950 scf/m) at 10 000 kPa (1,450 psi). National Association of Corrosion Engineers (NACE) certified equipment was employed to create an enclosed gas and liquids separation system. The sour return gas was recompressed down an existing pipeline to a gathering station approximately 10 km (6.2 miles). To ensure the safety of the rig floor personnel, the drillstring was purged with an inert gas to the top float, and then bled off back to a low pressure separation system for drillstring connections.The well was successfully drilled underbalanced for 21 days, with 1.3% (8.5 E(3)M(3))(0.3 MMscf) of the cummulative gas being flared. The use of recycled and recovered natural gas has economic benefits when compared to conventional disposable inert gas supplies, especially on a project basis.
机译:2005年,在加拿大南部的南部的原始,环境敏感的地区设计和钻井,设计和钻井间卧室。客户有两个主要驱动因素。之一是保持储层压力下整个钻井和完井操作和第二驱动器是安全地恢复9.0%的硫化氢(H(2)S)产气和再循环的H(2)S污染钻井液。该井未被分类为关键的酸,因为它靠近居民区和0.015 E(3)M(3)/千帕(0.37万立方英尺/ psi)的一个低井产的;然而,240 E(3)M(3)(8.5百万标准立方英尺)累计燃烧极限是由阿尔伯塔能源与公用事业委员会(EUB)罚款。壳体和孔尺寸在确认井中可以成功钻井底层膨胀到总深度(TD)后进行了优化。整合井工程和工艺工程都集成了整合过程和设备,以适应酸井流出物,同时控制井下多相流和压力环境。用于欠平衡部分中的注入气体经由现场从销售质量气体供给管压缩在高达的速率在10 000千帕(1450磅)提供给55 SM3 /分(1950标准立方英尺/米)。国家腐蚀工程师协会(NACE)认证设备采用了封闭的气体和液体分离系统。酸返回气体将现有的管道重新压缩到聚集站约10公里(6.2英里)。为了确保钻台人员的安全,钻柱用惰性气体吹洗以顶部浮子,然后排放掉回低压分离系统,用于钻柱connections.The以及成功欠平衡钻井,持续21天,与1.3的累积性气体的%(8.5 E(3)M(3))(0.3百万标准立方英尺)被张开。与传统的一次性惰性气体供应相比,使用回收和回收的天然气具有经济效益,特别是在项目基础上。

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