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Advancement in Mechanical Manipulation Enables Pulling Forces of 60,000 lbs on E-line – Operational Experiences from Pulling Stuck Plugs and Tools

机译:机械操纵的进步使得能够在封堵塞和工具中拉动60,000磅的力量 - 操作体验

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Objectives/Scope: Accidental plug setting and stuck tools is a cause of great frustration, operational delays and ultimately deferred production. A cost-efficient and swift resolution is always desired. This paper presents a new development in engineering in the form of a hydraulic stroking tool with the ability to apply 60,000 lbs of force. The tool has already been applied in the North Sea; lessons learned from these recent operations are disclosed in this paper. Methods, Procedures, Process: In one operation, a plug was accidentally set across the Christmas- Tree (XMT) and blowout preventer (BOP), effectively eliminating the XMT as a well barrier element and constituting a serious HSE risk. Conventional solutions failed to release the plug due to an insufficient pull force and then a failing jar.In another well, the setting tool had malfunctioned, resulting in a partially set plug and a stuck tool. Repeated attempts with heavy duty fishing equipment had damaged the fishing neck, further complicating the fishing operation as the seting tool had failed before it could break the stud connecting to the plug. Results, Observations, Conclusions: The high performance of the recently developed stroking tool turned out to be the solution to save both of these demanding operations. In the first well, it was estimated that the force required to shear the plug from the setting tool would be 43,300 lbs. The operation was completed in three runs with no misruns, which saved the operator from prolonged exposure to HSE risk, including well control situation.In the second well, the force required to shear the stud and free the setting tool was 40,000 lbs. Two release devices were combined in the toolstring, one below the hydraulic stroker and one below the cable head in order to allow further contingencies to mitigate risk and increase safety. After four attempts, the shear stud parted, thus completing the setting sequence and freeing the stuck setting tool. The operator got the well back on track, saved five days of rig time and avoided the costs of a workover rig.
机译:目标/范围:意外插头设置和卡住工具是一种令人沮丧,运营延误和最终推迟生产的原因。总是需要一种成本效益和快速的分辨率。本文以液压划分工具的形式提供了一种新的开发,具有施加60,000磅力的能力。该工具已应用于北海;本文披露了从这些最近的操作中汲取的经验教训。方法,程序,过程:在一个操作中,意外地将插头划过圣诞树(XMT)和井喷防喷器(BOP),有效地消除了XMT作为孔屏障元素,并构成严重的HSE风险。传统的解决方案由于拉力不足,然后在另一个井中而导致的塞子未能释放塞子,因此设置工具发生故障,导致部分设置的插头和卡住工具。重复尝试重型捕鱼设备已损坏捕鱼颈部,进一步使捕鱼操作变得复杂,因为设置工具在它可能会破坏连接到插头之前。结果,观察结论:最近开发的抚摸工具的高性能证明是保存这两种苛刻操作的解决方案。在第一井中,估计从设置工具中剪切插头所需的力将是43,300磅。该操作完成三次运行,没有误判,从长远地暴露于HSE风险,包括井控制情况,包括井下的风险,包括井控制的情况。在第二孔中,剪切螺柱和自由设定工具所需的力为40,000磅。将两个释放器件组合在工具序中,一个下方的液压型股:一个下方的电缆头部,以便允许进一步的突发事件来减轻风险并提高安全性。在四次尝试之后,剪切螺柱分开,从而完成设置序列并释放卡住的设定工具。操作员恢复轨道,节省了五天的钻机时间,避免了工作台的成本。

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