首页> 外文会议>SPE/EAGE European Unconventional Resources Conference >Case Study—Investigating Probable Root Causes Behind Consistent Higher Water Cut in a Mother CBM Well than its Deviated Wells:Well Spacing,Well Stimulation,and Overlying Strata Viewpoints and Recommendations
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Case Study—Investigating Probable Root Causes Behind Consistent Higher Water Cut in a Mother CBM Well than its Deviated Wells:Well Spacing,Well Stimulation,and Overlying Strata Viewpoints and Recommendations

机译:案例研究调查可能的根本原因在CBM母亲中切割的始终如一的较高水分,远远超过其偏离井:井间距,刺激,覆盖的地层观点和建议

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Production from coalbed methane(CBM)reservoirs can often be challenging,particularly related to the dewatering process. Improper positioning and completion of wells can lead to increased complications during the production phase.Additionally, consistently high water levels(undeclined static reservoir pressure)can impede gas production.This paper describes well and production information from the Raniganj coal block. The pad completion discussed has a mother vertical well(V-well)in which three main coal seams were completed(of the total five main seams with interspersed local seams),and dewatering commenced in 2009.At the end of 2011,encircling the V-well,four deviated wells(D-wells)at different azimuths were positioned at horizontal closures of 263 to 364 m from the bottom seam of the V-Well,wherein five main coal seams,along with interspersed local seams,were completed and scheduled for dewatering in mid-2012.Despite consistent high water production rates from the V-Well,the water levels in the V-Well stood consistently higher(rising upward)than the water levels in the D-wells,unlike nearby V and D-well pads. Well spacing information,well stimulation plots,perforation plans,and overlying strata for all five wells on this pad were studied and conclusions were drawn.This paper discusses such conclusions as well as the analyses performed to understand these issues.An attempt has also been made to best optimize hydraulic fracturing(HF)treatment designs to obtain the maximum benefits from stimulation operations. The results reported in this paper will influence the operator’s cost optimization,which could be a major positive influence on the low-cost CBM market in addition to increasing efficiency of the entire operation.
机译:煤层气(CBM)水库生产通常具有挑战性,特别是与脱水过程有关。在生产阶段期间,井的定位不当和完成可能导致复杂性增加。加法,始终如一的高水位(未卷积的静态储层压力)可以阻碍气体生产。本文描述了来自Raniganj煤炭块的井和生产信息。讨论的垫完成具有母垂直井(V-Well),其中三个主要煤层完成(总有五个主要接缝的主要接缝),并在2009年开始脱水。2011年底,环绕v - 距离不同方位角的四个偏离的孔(D-Wells)距离V孔井的底部接缝的水平封闭件,其中五个主煤层以及穿插局部接缝,并计划对于2012年中期的脱水。符合V-Wont的一致高水位产率,V阱中的水位始终如一(上升),而不是D-Wells中的水平,与附近的V和D-不同垫垫。研究了该垫上所有五个井的井间距信息,良好的刺激图,穿孔计划和覆盖地层,并得出结论。本文讨论了此次结论以及进行了解这些问题的分析。也已经尝试了为了最佳优化液压压裂(HF)处理设计,以获得刺激操作的最大益处。本文报告的结果将影响运营商的成本优化,除了增加整个运作的效率之外,还可以对低成本CBM市场进行重大积极影响。

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