首页> 外文会议>IADC/SPE Managed Pressure Drilling Underbalanced Operations Conference >Overcoming a 0.35 ppg Mud Weight Window - A Case History of Successful Automated Managed Pressure Drilling and Managed Pressure Cementing Offshore Malaysia
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Overcoming a 0.35 ppg Mud Weight Window - A Case History of Successful Automated Managed Pressure Drilling and Managed Pressure Cementing Offshore Malaysia

机译:克服0.35 PPG泥浆窗口 - 以马来西亚近海地区成功的自动化管理压力钻井和管理压力的案例历史

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TA is an over-pressurized well in the field development project located Offshore Peninsular Malaysia. Although the well was drilled as a development well, it also had an exploration objective as it was the first to penetrate the over pressured zones across a fault in the TA field. An initial attempt to drill conventionally resulted in severe gain and loss scenarios across the first of three sands 80 m below the 7” casing shoe, primarily due to weak coal formations. After many attempts to control losses, it was decided to plug- abandon the 6” open hole and to temporarily suspend the well due to insufficient operating window to drill ahead. After a year of suspension, a new drilling approach using a statically underbalanced mud weight (MW) in combination with an Automated Managed Pressure Drilling (MPD) system was introduced as the best solution for drilling into the well objectives. During the planning stage, different scenarios were analyzed based on the formation fracture gradient (FG) and pore pressure (PP) estimations. MPD plans were designed based on statically underbalanced mud while drilling, running the liner, and during the cementing job. During drilling, Dynamic Flow Checks (DFC) and Dynamic Formation Integrity Tests (DFIT) were performed using the MPD system to identify and confirm operating window. The target total depth was successfully reached with mud weighted within the narrow 0.35 ppg drilling window (17.8 - 18.1 ppg). Decision was then made to top kill the well at 1200 m-MDDF with 18.30 ppg mud, providing an overbalanced condition of 85 psi. Open hole logging operations were then successfully executed. The well was then displaced to a 16.30 ppg mud prior to performing Managed Pressure Cementing (MPC). This technical paper aims to discuss all of the MPD - MPC challenges faced and best practices developed during both the planning and execution stages of the program.
机译:TA是一个过压在位于近海马来西亚半岛的油田开发项目的顺利。虽然井所钻的发展,它也有一个探索的目标,因为它是第一个渗透跨断层在高压区在TA领域。初次尝试演练常规导致横跨第一三个砂80米7” 套管鞋下面,主要是由于弱煤地层严重增益和损失的情况。许多试图控制损失后,决定放弃插件6” 开洞,暂时中止以及由于操作窗口不足提前演练。在中断一年后,使用与自动控压钻井(MPD)系统组合的静态欠平衡泥浆重量(MW)的新钻井方法被引入作为钻入以及目标的最佳解决方案。在规划阶段,不同的方案是基于地层破裂梯度(FG)和孔隙压力(PP)的估计进行分析。 MPD计划是基于静态欠平衡钻井泥浆设计钻井时,运行内衬和固井作业期间。在钻井过程中,动态流量校验(DFC)和动态形成完整性测试(DFIT)使用MPD系统来识别和确认的操作窗口进行。 ( - 18.1 17.8 PPG)目标总深度成功的窄0.35 PPG钻孔窗口内加权泥浆到达。决定于是向顶杀所作的井在1200 M-MDDF与18.30 PPG泥浆,提供了85磅的过平衡状态。裸眼测井作业然后成功执行。然后该井移位至16.30 PPG泥执行控制压力固井(MPC)之前进行。此技术文件旨在讨论所有的MPD的 - MPC面临的挑战,并在方案的规划和执行阶段,发达国家的最佳做法。

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