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Formation Reason and Improvement Measure for Surface Defects of 0Cr18Ni10Ti Stainless Steel

机译:0Cr18Ni10TI不锈钢表面缺陷的形成原因及改进措施

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The formation reson of the surface defect of 0Cr18Ni10Ti after rolling is analyzed, some improving solutions are performed for avoiding the surface defect and enhancing the production quality. The investigation shows that the surface defect of rolled steel is mainly ascribed to the inclusions containing Ti, and TiO_2 and TiN is a primary source of inclusions in the steel. An effective way of reducing the inclusion performed is decreasing the Ti and N content in liquid steel. By appropriately increasing the carbon content of molten steel entering into the AOD, decreasing the carbon content of the end of blasting oxygen, slag skimming in the ladle and slagging in LF furnace, feeding SiCa wire before Ti alloying in LF furnace and optimization of Ti alloying method and protection casting with no oxidation, the yield of Ti is greatly increased, the TiO_2 and TiN inclusions is controlled better, the quality of products 0Cr18Ni10Ti all are greatly improved. The number of continuous casting furnace is increased from one to the three furnace, and the production efficiency is obviouly enhanced in TISCO.
机译:分析了轧制后0Cr18Ni10TI的表面缺陷的形成共振,进行了一些改进的溶液,以避免表面缺陷并提高生产质量。研究表明,轧制钢的表面缺陷主要归因于含有Ti的夹杂物,而TiO_2和锡是钢中的夹杂物的主要源。减少夹杂物的有效途径正在降低液体中的Ti和N含量。通过适当地提高进入AOD的钢水的碳含量,降低爆破氧气结束的碳含量,在LF炉中溅脱脂,在LF炉中喂养SICA线,在LF炉中合金化和Ti合金化优化。无氧化的方法和保护铸造,Ti的产率大大增加,TiO_2和锡夹层更好,产品质量0Cr18Ni10Ti均得到大大提高。连续铸造炉的数量从一个到三个炉子增加,而在蒂峡中,生产效率明显增强。

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