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TECHNOLOGICAL INNOVATIONS IN THE MITSUBISHI PROCESS TO ACHIEVE FOUR YEARS CAMPAIGN

机译:三菱流程中的技术创新实现四年的竞选

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The existing Mitsubishi Process line at Naoshima Smelter and Refinery has been operating successfully since 1991, and its present production capacity is 270,000tpy of copper. Furnace relining works have been carried out every two years to coincide with the compulsory bi-yearly boiler inspection, but the next target is to extend the furnace refractory life to four years, while still undergoing the mandatory boiler inspection every two years. Although the damage of hearth bricks beneath lances in the Smelting furnace was a matter of concern, it was reduced by controlling gas velocity and evening solid distribution to each lance. The life of bath level bricks in the Converting furnace was also a concern, but four-years continuous use of the bricks was achieved in the course of the last two campaigns. Several other improvements were also carried out to the cooling systems during the shutdown in 2005 to ensure longer campaign life. This paper summarizes recent improvements implemented to enhance the advantages of the Mitsubishi Process.
机译:在直岛冶炼厂现有三菱工艺线已成功运营自1991年以来,其本生产能力是铜的270,000tpy。炉大修工程已经进行了每两年与一致强制每两年锅炉检验,但下一个目标是到炉子耐火材料使用寿命延长到四年,而仍处于强制性锅炉检验每两年一次。尽管炉底砖喷枪下方在熔炼炉的损害是令人关注的问题,它是通过控制气体速度和晚上固体分配到每个矛形降低。沐浴水平砖在转炉寿命也是一个问题,但四年前连续使用的砖是在最后两个活动的过程中实现的。其他一些改善,在2005年关闭期间还开展了冷却系统,以确保更长的使用寿命运动。本文总结了实施,加强三菱工艺的优点最近有所改善。

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