首页> 外文会议>International Technical Conference on Clean Coal Fuel Systems >TDF Low NO_x Burner and Windbox Modifications for Emissions Control on a TURBO Furnace
【24h】

TDF Low NO_x Burner and Windbox Modifications for Emissions Control on a TURBO Furnace

机译:TDF低No_X燃烧器和涡轮炉上排放控制的风箱修改

获取原文

摘要

J.P. Madgett Station is located in Alma, Wisconsin. The boiler is a TURBO fired unit, manufactured by Riley Power Inc., a Babcock Power Inc. company (formerly Riley Stoker). The unit is designed to operate at a maximum continuous rating (MCR) of 2,700,000 pph of superheated steam at an outlet pressure of 1,900 psig and a temperature of 955°F. The reheater is designed for 2,425,000 pph of steam flow with an outlet pressure of 462 psig and outlet temperature of 955°F. This boiler was originally equipped with twenty-four (24) directional flame burners and four (4) Riley Ball Tube Mill pulverizers. The unit was designed to fire sub-bituminous coal. The burners were producing sustained NO_x emissions of 0.66 lb/MBTU with average CO emissions of 52 ppm. NO_x emissions needed to be reduced substantially to meet regulation requirements. Dairyland Power Cooperative contracted Riley Power Inc. to retrofit the unit with twenty-four (24) Tilting Directional Flame (TDF) Burners and Windbox modifications to improve NO_x emissions control. The aim was to achieve post-retrofit NO_x emission levels of ≤ 0.331 lb/MBtu over the range of loads, while maintaining CO emissions below 100 ppm and unburned carbon (UBC) levels below 1% by weight. The modifications to the combustion system associated with the TDF low NO_x burner installation combined with mill system tuning/optimization to improve coal flow distribution between burner lines resulted in a final NO_x emission of 0.271 lb/MBtu, an overall reduction of more than 18%. And, this level of NO_x reduction was achieved without the use of an overfire air system. Furthermore, the CO emissions and UBC levels were below the specified requirements with CO at 69 ppm (at 3% O_2) and UBC less than 1% by weight. This paper will describe the TDF burner design, modifications made to the windboxes, adjustments made to the existing mill system, start-up issues, and final results.
机译:J.P. Madgett Station位于威斯康星州阿尔马。锅炉是一款由Riley Power Inc.制造的涡轮机燃烧单位,Babcock Power Inc.公司(前身莱利·斯托克)制造。该装置设计成在1,900psig的出口压力和955°F的温度下在800,000pph的最大连续额定值(MCR)的最大连续额定值(MCR)。再热器设计为2,425,000磅的蒸汽流量,出口压力为462psig和955°F的出口温度。这款锅炉最初配备了二十四(24)个定向火焰燃烧器和四(4)个莱利球管磨机粉碎机。该装置设计为消防亚沥青煤。燃烧器生产持续的NO_X排放为0.66磅/ MBTU,平均共同排放为52ppm。 NO_X排放需要减少,以满足规定要求。 Dairyland Power Cooperative Contracted Riley Power Inc.用二十四(24)个倾斜定向火焰(TDF)燃烧器和风箱改造来改造单位,以改善NO_X排放控制。目的是在载荷范围内实现≤0.331LB/ MBTU的改造后NO_X排放水平,同时保持低于100ppm和未燃烧的碳(UBC)水平低于1%重量的CO排放。对与TDF低NO_X燃烧器安装相关联的燃烧系统的修改与轧机系统调谐/优化相结合,以改善燃烧线之间的煤流量分布,导致最终NO_X排放为0.271磅/ MBTU,总计超过18%。并且,在不使用过速空气系统的情况下实现了这种水平的NO_X。此外,CO排放和UBC水平低于CO以69ppm(3%O_2)和UBC小于1重量%的指定要求。本文将描述TDF燃烧器设计,对风箱进行的修改,对现有轧机系统,启动问题和最终结果进行的调整。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号