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Implementation of Electronic Detonators at Barrick Goldstrike Mines, Inc

机译:在Barrick Goldstrike Mines,Inc的实施电子雷管

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In March of 2001 Barrick Goldstrike Mines, Inc. began evaluating the potential benefits of electronic detonators at the Betze Post open pit gold mine. The original evaluation focused on increased fragmentation, and excavator productivity. During the original evaluation there was an attempt to quantify mill throughput. Early tests indicated that there would be a benefit to mill throughput, however management was hesitant to take on the added cost of electronic detonators based on the initial evaluation. In early 2002 a decrease in mill throughput was being forecast as a result of harder ore being encountered. As a result of the initial electronic detonator evaluation a team of individuals from the Open Pit and Process areas worked closely on the Drill-to-Mill (D2M) Continuous Improvement initiative. This initiative was targeted at improving mill throughput as the harder ores were encountered. Batch tests were conducted to determine if adjustments to drilling and blasting in the open pit could increase mill throughput and justify a 50% increase in drilling and blasting costs for the harder ore material. Mill throughput was increased through: 1) The use of electronic detonators allowing for high-speed precise timing. 2) Increased shock energy through the use of a high VOD Ammonium Nitrate. 3) Improved explosive distribution by decreasing pattern spacing and hole diameter. Digital analysis, plant operating data, and circuit surveys were used to quantify the gains in mill throughput. A micro-fracture analysis of the blasted material was also conducted using a scanning electron microscope. There was clear evidence of micro-fractures in the D2M material. The results of the batch tests indicated that an increase in mill throughput of 5% to 10% could be attributed to the optimized drilling and blasting techniques using electronic detonators. A rock response study was conducted in order to optimize the delay intervals to produce the best fragmentation in the D2M material. Four test blasts were monitored to define rock mass response, and four methods were used to determine the range of P-wave or seismic velocity of the D2M material. Based on the results of these tests a range of delay intervals between holes in a row and the delay interval between rows has been effectively defined. The resulting optimized delay intervals would not be possible without the use of electronic detonators. As a result of the D2M Continuous Improvement initiative the Barrick Goldstrike management team made an economic based decision to implement the use of electronic detonators along with the high VOD Ammonium Nitrate in the ore. The recognized gain in mill throughput offset the increase in drilling and blasting costs.
机译:2001年3月,2001年3月,Inc。开始评估电子戒断器在德雷斯露天坑金矿的潜在好处。原始评估专注于碎片增加和挖掘机生产率。在原始评估期间,试图量化轧机吞吐量。早期测试表明,对MILL吞吐量有益处,但管理层犹豫不决,以根据初始评估来承担电子雷管的增加的成本。 2002年初,由于难以遇到的矿石而导致磨机吞吐量减少。由于初始电子雷管评估,来自露天坑和工艺领域的个体团队紧密地致力于钻头 - 磨机(D2M)的连续改进倡议。随着难以遇到的矿石,该举措旨在改善轧机产量。批量测试以确定是否调整钻井和在露天爆破可以提高磨机产量和证明钻井增加了50%和爆破成本为较硬的矿石材料。轧机吞吐量通过:1)使用电子雷管允许高速精确定时。 2)通过使用高vod硝酸铵来增加休克能量。 3)通过降低图案间距和孔径来改善爆炸性分布。数字分析,工厂操作数据和电路调查用于量化轧机吞吐量的增益。还使用扫描电子显微镜进行喷砂材料的微断裂分析。 D2M材料中微骨折有明显的证据。批试验的结果表明,在通过磨机的5%至10%的增加可以归因于优化的钻孔和使用电子雷管爆破技术。进行岩石反应研究以优化延迟间隔以产生D2M材料中的最佳碎片。监测四种测试喷砂以定义岩体响应,并使用四种方法来确定D2M材料的P波或地震速度的范围。基于这些测试的结果,已经有效地定义了一行之间的孔之间的延迟间隔范围和行之间的延迟间隔。在不使用电子雷管的情况下,不可能实现所得到的优化延迟间隔。由于D2M持续改进倡议,Barrick Goldstrike管理团队通过矿石中的高vod铵硝酸铵以及矿石中的高vod铵硝酸铵进行了经济的决定。 MING吞吐量的公认增益抵消了钻井和爆破成本的增加。

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