首页> 外文会议>31st AIAA/ASME/SAE/ASEE Joint Propulsion Conference and Exhibit July 10-12, 1995/San Diego, CA >Improvement of Flow Quality in Turbine Engine Test Cells by the Elimination of Bellmouth-Induced Core-Flow Vortices
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Improvement of Flow Quality in Turbine Engine Test Cells by the Elimination of Bellmouth-Induced Core-Flow Vortices

机译:通过消除Bellmouth引起的核心流涡流来改善涡轮发动机测试室的流动质量

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With aircraft propulsion systems being required to meet more stringent requirements, test facilities are also required to provide more accurate information on these engines. Hence, a flow quality improvement program was conducted at AEDC to determine the cause of total pressure losses at the bellmouth exit. The initial premise for the cause of the total pressure losses in certain direct connect tests was bellmouth inlet vortics. In addition, a program was conducted to evaluate the use of conical extensions to eliminate any bell-mouth-induced vortices and to develop design duidelines for bellmouth extensions to include such parameters as radial gap, axial gap, and extension angle.
机译:由于需要飞机推进系统来满足更严格的要求,因此还需要测试设备来提供有关这些发动机的更准确的信息。因此,在AEDC进行了流量质量改进计划,以确定喇叭口出口处总压力损失的原因。在某些直接连接测试中造成总压力损失的最初前提是喇叭口进气涡流。此外,还进行了一个程序,以评估圆锥形延伸部的使用以消除任何由钟形口引起的涡流,并为喇叭形延伸部开发设计导图,以包括诸如径向间隙,轴向间隙和延伸角之类的参数。

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