首页> 外文会议>Annual Indonesian Petroleum Association convention and exhibition >UTILIZATION OF CASED-HOLE LOGGING FOR PRODUCTION OPTIMIZATION: A CASE STUDY FROM INA FIELD-SOUTH EAST SUMATRA BLOCK
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UTILIZATION OF CASED-HOLE LOGGING FOR PRODUCTION OPTIMIZATION: A CASE STUDY FROM INA FIELD-SOUTH EAST SUMATRA BLOCK

机译:利用套管测井技术进行生产优化:以INA田南东苏门答腊区块为例

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Maximizing production and realizing optimal oil recovery becomes increasingly difficult as in-field drilling is less viable because of production history and economic issues. Thus optimization of production in existing wells by production enhancement and reevaluation of reservoir potential is increasingly important to contractor's cash flow and ultimate production profile. Petroleum engineers and geologists know reservoir characteristics from original well logs, but present rock properties and well conditions can only be determined from new cased-hole logs.During 2008-2009, cased-hole logs were run in five wells in CNOOC's Southeast Sumatra Ina Field -Ina E-07, Ina E-08, Ina T-01, Fara B-01, and Fara B-03. Based on log interpretation, several action plans were recommended to optimize production. The recommendations included additional perforations, squeeze cementing to shut-off water and gas, and re-perforation of some producing intervals.Remedial work based on cased-hole logging resulted in significantly improved production at Ina E-07 well. Ina E-07 has several intervals open and it was urgent to determine the interval producing gas since this well is lifted by electrical submersible pump (ESP). The problem zone was identified from cased-hole logs and isolated. Since then, Ina E-07 has been closely monitored. The amp chart now displays a smooth trend indicating the gas has been successfully isolated. Since remedial work, the well is producing 250-300 BOPD continuously compared to intermittent production before work over. Current pump life is 193 days compared to 70 days and 17 days from previous pumps. Economics are favorable as intervention costs of $241,000 have resulted in production of 38 MBO compared to two previous well interventions that cost $385,000 and yielded 22 MBO (run life and production as per November 19, 2009).The success of the field review and reevaluation has been discussed at the communication forum between contractor and government agency with the contractor now being encouraged to implement the remainder of the action plans to optimize production. Cased-hole logging is a valuable, cost effective tool for optimizing production in mature fields.
机译:由于生产历史和经济问题,由于野外钻井的可行性降低,最大化产量和实现最佳采油率变得越来越困难。因此,通过提高产量和重新评估储层潜力来优化现有井中的产量,对于承包商的现金流量和最终生产状况越来越重要。石油工程师和地质学家可以从原始的测井资料中了解储层特征,但是目前的岩石特性和井况只能从新的套管井测井资料中确定。 在2008年至2009年期间,中海油在苏门答腊岛东南部伊那油田(Ina E-07,Ina E-08,Ina T-01,Fara B-01和Fara B-03)的5口井中进行了套管井测井。根据对原木的解释,建议了一些行动计划以优化生产。这些建议包括增加射孔,挤压固井以切断水和天然气,以及对某些生产层段进行射孔。 基于套管井测井的补救工作显着提高了Ina E-07井的产量。 Ina E-07有几个开放的时间间隔,因此迫切需要确定生产天然气的时间间隔,因为该井是由电潜泵(ESP)提起的。从套管井测井中识别出问题区域并加以隔离。从那以后,Ina E-07受到了密切监视。现在,安培图表显示出平滑的趋势,表明已成功隔离气体。由于进行了修复工作,与修井前的间歇生产相比,该井连续生产250-300 BOPD。当前的泵寿命为193天,而以前的泵为70天和17天。经济学上是有利的,因为干预成本为241,000美元,导致生产了38 MBO,而之前的两口井干预成本为385,000美元,产生了22 MBO(根据2009年11月19日的运行寿命和产量)。 在承包商与政府机构之间的交流论坛上讨论了现场审查和重新评估的成功之处,现在鼓励承包商实施其余的行动计划以优化生产。套管井测井是在成熟领域优化生产的有价值,具有成本效益的工具。

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