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In-Plant Piping Hydrogen Induced Cracking Survey in a Gas Oil Separation Plant (Case Study)

机译:瓦斯油分离厂的厂内管道氢致裂纹调查(案例研究)

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A detailed survey of Hydrogen Induced Cracking (HIC) was conducted in a Saudi Gas Oil Separation Plant (GOSP). The piping system was not originally fabricated using HIC resistant steel and has been employed in wet sour crude and gas services for the last 24 years. This particular GOSP was built in 1982. It produces 300 thousand barrels oil per day (MBOD) of crude; and 100 million standard cubic feet per day (MMscfd) of associated sour gas. There were 170 pipe spools that were identified with HIC in the GOSP facilities using ultrasonic on-stream inspection (OSI). The objective of this survey was to inspect, monitor and identify severely effected plant piping to avoid occurrence of any catastrophic failure that could result from HIC damage. Indications of HIC, categorized as moderate to severe with continuous loss of back wall reflection, have been recorded for many pieces of equipment and piping spools.Additionally advanced ultrasonic examination (P-scan ultrasonic mapping), which is used to detect corrosion, laminations, inclusions, HIC/blistering and any defect between the outer surface and the internal surface, has been performed. This inspection was recently conducted on selected locations to provide more detailed information for a risk based assessment (RBA) review. Based on the result of this assessment, pipe replacement will be deferred by 2 years; and significant cost savings through production loss avoidance will be realized. Potential short-term repair measures, including full metallic sleeves and non-metallic composite wrapping, to extend the service life of the affected piping until the next scheduled test and inspection T&l, are being considered as alternatives if stepwise cracking develops in the future.
机译:在沙特瓦斯油分离厂(GOSP)中进行了对氢诱导裂化(HIC)的详细调查。管道系统最初不使用HIC耐钢制造,并在过去的24年中用于湿酸原油和天然气服务。这个特殊的GOSP建于1982年。它每天生产300万桶油(MBOD)原油;和100万标准立方英尺/天/天(MMSCFD)的相关酸性气体。使用超声波on-Stream检验(OSI),在GOSP设施中鉴定了170个管道线轴。本调查的目的是检查,监测和识别严重的植物管道,以避免发生任何可能由HIC损坏引起的灾难性故障。 HIC的适应症被分类为中度至严重,随着后壁反射的连续损失,已经记录了许多设备和管道线轴。 另外,已经进行了先进的超声波检查(P扫描超声波映射),用于检测腐蚀,层压,夹杂物,HIC /起泡和外表面和内表面之间的任何缺陷。最近在选定地点进行了此检查,以提供基于风险的评估(RBA)审查的更详细信息。根据该评估的结果,搬运站将被推迟2年;将实现通过生产损失避免的显着节省成本。潜在的短期修复措施,包括全金属套管和非金属复合包装,以延长受影响管道的使用寿命,直到下一个预定的测试和检查T&L被视为替代方案,如果在未来发展。

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