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Two Years After First Oil Paraffin and Scale Flow Assurance Management – Lessons Learned

机译:第一次油石蜡和规模流量保证管理两年后 - 经验教训

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This paper describes the evaluation of paraffin and scale risk management based on real production samples, and how this differed to the assumptions made during the basis of design. The production facility has two unmanned tiebacks with a field total of just under 20 wells. For first oil the paraffin and scale management strategy, like most of the flow assurance strategy, was based on pre-production samples. Two years after first oil, almost all the wells were sampled – the first such exercise of it’s kind – gathering large and representative chemical free crude oil and produced water. Produced water samples were analyzed enabling a system-wide scale review for production wells, departing pipelines and major processing vessels and equipment. Some scale had already been observed in the process, in the hydrocyclones and heat exchangers, and this evaluation helped to highlight the other key risk areas and develop appropriate mitigation strategies – not based on pre-production data and samples. This aided the operator in instigating a more robust scale inhibitor injection strategy, in particular for the subsea in-field flow lines. The areas identified as having a paraffin deposition risk in the field were the fluids arriving from the subsea tiebacks where the arrival temperatures were lower than the cloud points. Cold finger testing identified that greater than 60% inhibition efficacy was realized when 10 to 50 ppm of the incumbent wax inhibitor was used. Details are given on some of the shortcomings in the chemical injection system, capturing the lessons learned in control of wax and scale inhibitor distribution through the subsea injection system. Information is given on how this was countered using the most efficient and cost effective chemical mitigation strategy. Practical advice is then offered on how to better interpret pre-production samples to better predict and design flow assurance strategies prior to first oil.
机译:本文介绍了基于实际生产样本的石蜡和规模风险管理的评估,以及如何与在设计基础上进行的假设不同。生产设施有两种无人机的重建,距离20井之外的田野。对于首次油石蜡和规模管理策略,如大多数流动保证策略,都是基于预生产样本。第一次油后两年,几乎所有的井都被取样 - 首先是它善良的运动 - 收集大型和代表性的化学物质原油和产水。分析了生产的水样,为生产井,脱水管道和主要加工船舶和设备提供了系统范围的规模审查。在水力旋流器和热交换器中,在该过程中已经观察到了一些规模,并且该评估有助于突出其他关键风险区域,并制定适当的缓解策略 - 而不是基于预生产数据和样本。这辅助操作员在唤起更强大的尺度抑制剂喷射策略,特别是用于海底流动线。鉴定为具有该领域的石蜡沉积风险的区域是从抵达温度低于云点的海底连接到达的流体。当使用10至50ppm的现有蜡抑制剂时,实现了冷手指测试,在使用10至50ppm时,实现了大于60%的抑制效果。详细说明了化学注射系统中的一些缺点,捕获了通过海底注射系统控制蜡和尺度抑制剂分布的经验教训。有关如何使用最有效和具有成本效益的化学缓解策略对抗的信息。随后提供了如何更好地解释生产预先预测和设计第一油的预测和设计流动保证策略。

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